Subject: [FlyRotary] Re: Bill Eslick's EC2 inspection
My own experience is that when the
cold start switch is inappropriately selected and the
engine is running at medium-hight rpm - is that the
engine does not stop immediately, but starts to bog
down, sloppy sounding exhaust and then eventually dies.
But, then I am using 460 cc/min injectors. I even found
that I could fly (keep engine running) with the cold
start on provided I put the manual mixture control
maximum lean and it was still sloppy sounding - if I had
550 cc/min injectors I doubt that it would have kept
running.
My best SWAG given that Tracy found
no fault and the sudden termination of the engine - is
either CAS problem or ignition (and it would have to be
an ignition problem that would taken out both sets of
spark producing devices). If CAS then that could
account for the sudden stoppage more so than a misplaced
cold start switch in my opinion, but then distant
diagnostics is still an evolving "Art". {:>)
Ed
Sent: Saturday, October 15, 2011 3:32 AM
Subject: [FlyRotary] Re: Bill Eslick's EC2
inspection
Man, I hate that cold start switch ;-)
Dave Leonard
On Fri, Oct 14, 2011 at 1:02 PM,
Tracy
<rwstracy@gmail.com>
wrote:
Thought the group would like to hear
what i found when I Finally had a chance to closely
examine Bill's EC2. I was hoping to find a definitive
reason behind his sudden and complete loss of power on
takeoff on his last flight.
On powering it up on the bench I found both A and B
controllers Working normally. Bill noted in his report
that in the 'Fly The Plane' situation called for in a
power failure during takeoff he had not tried switching
to controller B. It does not appear that it would have
done any good this time.
None of the parameters were set outside the expected
range so no sign of data corruption. In fact the only
thing notable about the data downloaded from it was the
unusually smooth programming of the MAP table. Most of
the time I find units returned for updates with choppy
looking data in the table indicating a lack of care or
proper methodology in setting it up. A and B
controllers had identical data.
The PCM was also returned with the unit so just in case
the control panel was the cause I substituted it for the
bench test panel I normally use. Thought I saw a
problem because the injection pulse width was so large
that it could well have caused engine flooding. This
was caused by the mixture control being set fairly high
and the cold start switch being in the on position.
This does not prove anything because that could easily
have happened during removal of the panel from the plane
or while packing it for shipping. When the switch and
mixture control was returned to normal settings the
injection pulse width returned to normal.
Ran the unit on the bench for several hours while
heating and subjecting it to vibration but nothing else
turned up.
Tracy
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David Leonard
Turbo Rotary RV-6 N4VY
http://N4VY.RotaryRoster.net
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