X-Junk-Score: 0 [] X-Cloudmark-Score: 0 [] X-Cloudmark-Analysis: v=2.3 cv=G+5i7Os5 c=1 sm=1 tr=0 a=M2OdGcRFAffNL5OuQB6YSA==:117 a=jpOVt7BSZ2e4Z31A5e1TngXxSK0=:19 a=x7bEGLp0ZPQA:10 a=BaKdtXMH_38A:10 a=J70Eh1EUuV4A:10 a=pGLkceISAAAA:8 a=Ia-xEzejAAAA:8 a=UKPAHat8AAAA:8 a=o1OHuDzbAAAA:8 a=x-75qrxFAAAA:8 a=7g1VtSJxAAAA:8 a=-NXb0EheYxhm_Wu5G6QA:9 a=QEXdDO2ut3YA:10 a=4hVreLlt7OsA:10 a=Qa1je4BO31QA:10 a=K_Pv9SaLS-kA:10 a=gvSQh4r-fQ0A:10 a=a45UzwrQ_8uFqAkFH-IA:9 a=tvmjpg1v0PXl5uYq:21 a=Urk15JJjZg1Xo0ryW_k8:22 a=Fc6xXSS-RxGHxrvp76Qp:22 a=5YQ6H4ZxyGn-KoBYtt8s:22 a=pSfGKr4syse1NfsQC3dY:22 a=grOzbf7U_OpcSX4AJOnl:22 From: "William Schertz wschertz343@gmail.com" Received: from mail-io1-f54.google.com ([209.85.166.54] verified) by logan.com (CommuniGate Pro SMTP 6.2.14) with ESMTPS id 12916888 for flyrotary@lancaironline.net; Mon, 02 Sep 2019 15:27:08 -0400 Received-SPF: pass receiver=logan.com; client-ip=209.85.166.54; envelope-from=wschertz343@gmail.com Received: by mail-io1-f54.google.com with SMTP id d25so28399044iob.6 for ; Mon, 02 Sep 2019 12:27:08 -0700 (PDT) DKIM-Signature: v=1; a=rsa-sha256; c=relaxed/relaxed; d=gmail.com; s=20161025; h=mime-version:references:in-reply-to:from:date:message-id:subject:to; bh=U9wbI0mrin67jEVS13oDcPbr+nqfiUhgzpFF22z00fs=; b=Y5p+B9gsV1WhzbbPIEoqhbWvrLPG9IVApTnVUgy+bV06lBZgev2FOfLo+jKSjaFKcU hXQ+fRcS5M8Q+Tfn8FhYfp0PZKBtJH8eXnVVVW679yIoT8SIAqTKAgdtslLl3YgkMTll fNgvQU9LecWt2ybtLf8Lme3IJkIKJQORVkTejvaw1wnmZogNJxUzKswJL2GUwVQYT36S BdGxPAgNHDYzaw721FeEX9RAakkEK9BP4md1kfua5X7sIvWoUr4gijBe0rSBxFbZ/Jn+ dR40n8vMRWWjNhl6ARE6r0eQkV1NryxEAAZFs5NW9e4BH9hDf6DQ0yvVDeg9X50oEHkb ixOQ== X-Google-DKIM-Signature: v=1; a=rsa-sha256; c=relaxed/relaxed; d=1e100.net; s=20161025; h=x-gm-message-state:mime-version:references:in-reply-to:from:date :message-id:subject:to; bh=U9wbI0mrin67jEVS13oDcPbr+nqfiUhgzpFF22z00fs=; b=AFQXGRt+DgVY9ghF/4E64gAi2MNYhqhThS6jKXy4ku4Oc3H3xEQYF7R7EdiSEz9xw1 05MTTNvwIM6JLdMFUJwJqEwRwx74FfHmyl3p81pV4/bu+lMGi2MvJwqymEYMkeYTXdaq 1Kh5fndPlMSyUAoHDtTWABLNMUL/Wn9+Kby8F+EHHPDJXEO76F3F3rLNwJcYF3biM/gO irilh1x4P3kUI1qjf7OHH8y+bCqlJJEm32jShYxKv2ny+3zKA13HHtHhJerw3Ar/Al4a PXaSm+NSYfqdsrlFhu0z97pW+3eU8t0QqlLCqr8CETv8ALKHQ3KixFrUGX/F383U3tZN lcDA== X-Gm-Message-State: APjAAAXE96PopqH4UBj3wc7XHzeqCOaPi3Nhx0GNIFjy9EyA5E7oBLQ9 yRTxGmkFIJJSNX2qnjdsw2iyILekAJVIaELoHEAWGg== X-Google-Smtp-Source: APXvYqxNIXh/pV8c8uHsqJfUwGFu3YSQWvCaVbSp3g+a2Njp3L5SD1kyvKGSeSSgkz1GWaFbDeWp60sTUikAFnKb2pE= X-Received: by 2002:a5d:8d12:: with SMTP id p18mr3581266ioj.251.1567452410901; Mon, 02 Sep 2019 12:26:50 -0700 (PDT) MIME-Version: 1.0 References: In-Reply-To: Date: Mon, 2 Sep 2019 13:26:36 -0600 Message-ID: Subject: Re: [FlyRotary] Re: The Story of an unecessary rebuild To: Rotary motors in aircraft Content-Type: multipart/alternative; boundary="000000000000277ae3059196f42b" --000000000000277ae3059196f42b Content-Type: text/plain; charset="UTF-8" Dave If "running" to wear in the seals is needed, have you considered replacing the prop with a pulley and using an electric motor to turn the engine over for an extended period of time? Bill On Mon, Sep 2, 2019 at 10:04 AM David Leonard wdleonard@gmail.com < flyrotary@lancaironline.net> wrote: > Hi Bobby, most definately I had made sure the rotors were clear, along > with most of the other tricks (eh, except hot coffee). At this point I am > still 90% sure that the problem was low compression due to wear and tear. > > Now that I have completed the re-build add tested and/or replaced every > other component of the eletrical and fuel systems I am still convinced that > my problem is once again low compression (I cant get it to start at all > now). My leading theory is that during the rebuild I took Lynn's advise a > little too seriously and did not file down my side seals enough. Perhaps > if I can just get it started one time, those side seals will break-in > quickly and all will be good. But, more than likely I will need to remove > the engine from the plane again and take it apart just so I can get a file > on those side seals. While there I will also take some fine sand paper to > my new bearings so they are a little less tight. > > The act of writting that tale in electrons helped me to figure out my > ongoing woes, that are difficult to face because of the work involved in > another re-build. > > At this point it is an internal battle betweeen wanting my plane back and > not wanting to dive into another rebuild. Its a lot like childbirth. Over > time the pain of the rebuild will be forgotten and the desire for my plane > will increase to the point where I am ready to endure the proess again. > > I really thank everyone for the comments and input. It reassured me that > I was not missing something easy to fix that I had not thought of. > > David Leonard > Turbo Rotary RV-6 N4VY > 229 mph qualifying time at Reno 2011 (probably 300+ hp then) > 1100+ hours over 14 years flying > 6 rebuilds over the years, probably about to be 7. (But this was the > first time I replaced the iron side housings) > > > On Mon, Sep 2, 2019, 6:51 AM Bobby J. Hughes bhughes@qnsi.net < > flyrotary@lancaironline.net> wrote: > >> Dave, >> >> Have you attempted a hot start with the fuel pumps off to clear the >> engine? Leaking injectors after shutdown? >> >> Bobby >> >> Sent from my iPad >> >> On Aug 31, 2019, at 2:38 PM, Matt Boiteau mattboiteau@gmail.com < >> flyrotary@lancaironline.net> wrote: >> >> I have a fuel temp sensor on my fuel return. Actually it's a GM flex >> sensor, that detects ethanol % and gives temperature as a bonus. When I've >> shut down, I have seen the fuel temps climb to 120F (and probably more). It >> takes about 10-20seconds to turn on the fuel pump, to see the temperatures >> start to drop back down to 90F. >> >> Hard to start when the fuel temps that high on a hot engine. >> >> - Matt Boiteau >> >> On 2019-08-31 11:18:54 AM, Bobby J. Hughes bhughes@qnsi.net < >> flyrotary@lancaironline.net> wrote: >> I agree with Finn. Alternator noise would be my first guess. You could >> try adding a filter and dedicated ground from alternator back to FWF main >> ground point. Jumper cable for temporary ground wire. Hot fuel should not >> be possible with return lines. >> >> Bobby >> >> Sent from my iPad >> >> On Aug 31, 2019, at 8:01 AM, Finn Lassen finn.lassen@verizon.net < >> flyrotary@lancaironline.net> wrote: >> >> Tried to replace the alternator? >> >> Really good ground battery to alternator? >> >> Can you put an oscilloscope one the power to coils and supply line to the >> EC2? >> >> (I'm thinking noise from alternator. Some bad connection somewhere when >> hot.) >> >> You know, one way to troubleshoot intermittent electronic failures it to >> heat individual components up and/or cool down (a lot) until you find the >> intermittently bad component. >> >> Finn >> >> On 8/31/2019 1:19 AM, David Leonard wdleonard@gmail.com wrote: >> >> Interject when you figure out my underlying issue.?? Please! >> >> It started about a year ago.?? I was putting a lot of hours on N4VY >> (Turbo rotary RV-6) commuting for work.?? One day I flew to Ramona to meet >> up with my formation flying buddies.?? After the brief we went to start our >> planes but mine wouldn't start and I had to bow out of the flight.?? It >> would crank and almost catch, but I wore out my battery trying.?? After >> recharging for a couple hours it started up normally.?? I flew home and >> wrote it off as some sort of start procedure SNAFU.?? I use Tracys EC2. >> >> But that was the start of a long succession of difficult starts when >> pre-warmed, starting fine when cold.?? Sometimes leaving me stranded at a >> gas stop until the engine cooled.?? While in a safe place I tested air >> starts and there seemed to be no issue there just turning the fuel pumps >> back on with the prop spinning. >> >> Then it started doing something else strange.?? After starting it would >> run really rough?? whenever the alternator output got above 55amps or so.?? >> By rough I mean sputtering and resisting advancing the throttle by sagging >> and occasionally backfire.?? If I had been cranking for a long period it >> could take a minute for the amps to drop and the engine to run normally. >> >> I started by checking for loose wires and replacing the spark plugs. (No >> improveement) >> >> So then I replaced the battery, it still seemed strong but maybe the >> voltage was dropping with cranking or somethng.?? I got interested in Li >> Ion batteries and splurged on the Big one.?? It increased my total enerrgy >> storage, CCAs, and decreased weight by over 10#.?? Expensive but worth it >> considering they are also supposed to last longer. >> >> But it turns out the old battery was fine after.?? Not only did it not >> solve the problem, but because the Li Ion battery can take a much faster >> charge, it would max out the alternator at least briefly on EVERY start, >> making the problem worse. >> >> Next was fuel filter and spark plug wires, no improvement. >> >> The condition continued to slowly worsen despite trying richer mixtures >> of 2-stroke oil and or MMO.?? So I finally grounded it. >> >> My thought at this point was that the compression had finally deggraded >> to the point where compression was not enough for combustion unless turning >> really fast.?? Perhaps the extra drag from full output of the alternator >> made the condition worse.?? And when it was hot the rotor housings expanded >> just enough to really kill the compression.?? The side iron plates in that >> engine had the better part of 1000 flight hours plus unknown time in an >> RX7.?? Compression measured mid 20s on both rotors, for what thats worth.?? >> Time for a rebuild. >> >> I went all out.?? All new rotor and side housings, seals, springs, >> o-rings and the necessary aircraft mods to those parts.?? (fittings, >> etc..., EGR passages pluged)?? I also replaced the LS1 coils and the coil >> harness. >> >> And??? Nothing.?? Fuel flow and injector gross function verified.?? All >> sparks verified during cranking with a timing light.?? Tried a different >> CAS just for kicks.?? The engine is a little tight because it is new, >> compression is not spectacular cause the seals have not set, perhaps the >> apex seal little bits are still glued on.. >> >> Jump in here anytime. >> >> >> You know? You are right, I just need to disconnect the alternator and >> keep cranking until it finally catches and gets a little bit of a >> break-in.???? >> >> This talk has been really helpful for me. >> >> Dave Leonard >> (the forever optimist) >> Also going to switch to full synthetic 2-stroke oil without MMO.?? The >> new engine will never know how good it has it.?? >> >> >> >> On Thu, Aug 29, 2019, 10:18 PM Matt Boiteau mattboiteau@gmail.com < >> flyrotary@lancaironline.net> wrote: >> >>> Well ran into a little bit of a snag on my RX8 engine???. >>> While trying different things to cool down the oil, during high-speed >>> taxi tests I managed to blow out the temporary clear level tube on my >>> coolant expansion tank, which lead to pressure loss, which caused it to >>> overheat. Managed to shut down near the hanger and get a water hose on the >>> rads, but I feel the engine got baked underneath the fiberglass cowl. >>> *Future note, need to come up with some flaps that open after shutdown or >>> something, to let the heat escape out. Maybe even an electric fan that runs >>> for 5 minutes after shutdown* >>> >>> I know I blew some type of coolant gasket, but unsure if the irons are >>> warped. Going to take apart next weekend. Just wanted to run by my list of >>> mods, to see if I need to change anything or add/remove. >>> >>> 25hours, 99% ground testing >>> The iron plates were lapped and renitraded >>> Rotor housings were new and welded in P-Ports >>> RotaryAviation master kit (RA super seals) >>> >>> >>> *Oil *~125psi at full throttle >>> 20w50 VR1 high zinc >>> RX7 rear pressure regulator >>> 2 washers under front pressure regulator >>> weber jet kit >>> thermal pellet >>> >>> >>> >>> *Coolant *1.3bar cap >>> ECU says ~27psi at full throttle, not sure I believe that yet. Lots of >>> noise at full throttle on my pressure sensors (pic attached) >>> 70/30 Zerex G-05 >>> >>> ?? >>> >>> I???ll order the Atkins oring kit, supposedly their brown inner water >>> jacket seals can handle a bit higher temps. >>> https://www.atkinsrotary.com/store/04-11-Rx8-O-Ring-Kit-ARE317.html >>> >>> - Matt Boiteau >>> -- >>> Homepage:?? http://www.flyrotary.com/ >>> Archive and UnSub:?? ?? >>> http://mail.lancaironline.net:81/lists/flyrotary/List.html >>> >> >> --000000000000277ae3059196f42b Content-Type: text/html; charset="UTF-8" Content-Transfer-Encoding: quoted-printable
Dave
If "running" to wear in the seals is ne= eded, have you considered replacing the prop with a pulley and using an ele= ctric motor to turn the engine over for an extended period of time?
Bill

On Mon, Sep 2, 2019 at 10:04 AM David Leonard wdleonard@gmail.com <flyrotary@lancaironline.net> wrote:
=
Hi Bobb= y, most definately I had made sure the rotors were clear, along with most o= f the other tricks (eh, except hot coffee).=C2=A0 At this point I am still = 90% sure that the problem was low compression due to wear and tear.

Now that I have completed the re-buil= d add tested and/or replaced every other component of the eletrical and fue= l systems I am still convinced that my problem is once again low compressio= n (I cant get it to start at all now).=C2=A0 My leading theory is that duri= ng the rebuild I took Lynn's advise a little too seriously and did not = file down my side seals enough.=C2=A0 Perhaps if I can just get it started = one time, those side seals will break-in quickly and all will be good.=C2= =A0 But, more than likely I will need to remove the engine from the plane a= gain and take it apart just so I can get a file on those side seals.=C2=A0 = While there I will also take some fine sand paper to my new bearings so the= y are a little less tight.

The act of writting that tale in electrons helped me to figure out my on= going woes, that are difficult to face because of the work involved in anot= her re-build.

At this po= int it is an internal battle betweeen wanting my plane back and not wanting= to dive into another rebuild.=C2=A0 Its a lot like childbirth. Over time t= he pain of the rebuild will be forgotten and the desire for my plane will i= ncrease to the point where I am ready to endure the proess again.

I really thank everyone for the c= omments and input.=C2=A0 It reassured me that I was not missing something e= asy to fix that I had not thought of.

David Leonard
Turbo Rotary RV-6 N4VY
229 mph qualifying time at Reno 2011 (probably 300+ h= p then)
1100+ hours over 14 years flying
6 rebuilds over the years, probably about to be 7.=C2=A0 (But t= his was the first time I replaced the iron side housings)


On Mon, Sep 2, 2019, 6:51 AM Bobby J. Hughes bhughes@qnsi.net <flyrotary@lancaironl= ine.net> wrote:
Dave,

Have you attempted a hot = start with the fuel pumps off to clear the engine? Leaking injectors after = shutdown?

Bobby=C2=A0

Sent from my iPad

On Aug 31, 2019, at 2:= 38 PM, Matt Boiteau mattboiteau@gmail.com <flyrotary@lan= caironline.net> wrote:

I have a fuel temp sensor on my fue= l return. Actually it's a GM flex sensor, that detects ethanol % and gi= ves temperature as a bonus. When I've shut down, I have seen the fuel t= emps climb to 120F (and probably more). It takes about 10-20seconds to turn= on the fuel pump, to see the temperatures start to drop back down to 90F.= =C2=A0

Hard to start when the fuel temps that high on a hot engine.<= br>

- Matt Boiteau

On 2019-08-31 11:18:54 AM, Bobby J. Hughes bhughes@qnsi.net <flyrotary@lancaironline.net> wrote:

I agree with Finn. Alternator noise would be my first guess. You could= try adding a filter and dedicated ground from alternator back to FWF main = ground point. Jumper cable for temporary ground wire. Hot fuel should not b= e possible with return lines.=C2=A0

Bobby=C2=A0

Sent from my iPad

On Aug 31, 2019, at 8:01 AM, Finn Lassen finn.lassen@ver= izon.net <flyrotary@lancaironline.net> wrote:
=20 =20 =20 =20
Tried to replace the alternator?

Really good ground battery to alternator?

Can you put an oscilloscope one the power to coils and supply line to the EC2?

(I'm thinking noise from alternator. Some bad connection somewher= e when hot.)

You know, one way to troubleshoot intermittent electronic failures it to heat individual components up and/or cool down (a lot) until you find the intermittently bad component.

Finn

On 8/31/2019 1:19 AM, David Leonard wdleonard@gmail.com = wrote:
=20
Interject when you figure out my underlying issue.?? Please!

It started about a year ago.?? I was putting a lot of hours on N4VY (Turbo rotary RV-6) commuting for work.?? One day I flew to Ramona to meet up with my formation flying buddies.?? After the brief we went to start our planes but mine wouldn't start and I had to bow out of the flight.?? It would crank and almost catch, but I wore out my battery trying.?? After recharging for a couple hours it started up normally.?? I flew home and wrote it off as some sort of start procedure SNAFU.?? I use Tracys EC2.

But that was the start of a long succession of difficult starts when pre-warmed, starting fine when cold.?? Sometimes leaving me stranded at a gas stop until the engine cooled.?? While in a safe place I tested air starts and there seemed to be no issue there just turning the fuel pumps back on with the prop spinning.

Then it started doing something else strange.?? After starting it would run really rough?? whenever the alternator output got above 55amps or so.?? By rough I mean sputtering and resisting advancing the throttle by sagging and occasionally backfire.?? If I had been cranking for a long period it could take a minute for the amps to drop and the engine to run normally.

I started by checking for loose wires and replacing the spark plugs. (No improveement)

So then I replaced the battery, it still seemed strong but maybe the voltage was dropping with cranking or somethng.?? I got interested in Li Ion batteries and splurged on the Big one.?? It increased my total enerrgy storage, CCAs, and decreased weight by over 10#.?? Expensive but worth it considering they are also supposed to last longer.

But it turns out the old battery was fine after.?? Not only did it not solve the problem, but because the Li Ion battery can take a much faster charge, it would max out the alternator at least briefly on EVERY start, making the problem worse.

Next was fuel filter and spark plug wires, no improvement.

The condition continued to slowly worsen despite trying richer mixtures of 2-stroke oil and or MMO.?? So I finally grounded it.

My thought at this point was that the compression had finally deggraded to the point where compression was not enough for combustion unless turning really fast.?? Perhaps the extra drag from full output of the alternator made the condition worse.?? And when it was hot the rotor housings expanded just enough to really kill the compression.?? The side iron plates in that engine had the better part of 1000 flight hours plus unknown time in an RX7.?? Compression measured mid 20s on both rotors, for what thats worth.?? Time for a rebuild.

I went all out.?? All new rotor and side housings, seals, springs, o-rings and the necessary aircraft mods to those parts.?? (fittings, etc..., EGR passages pluged)?? I also replaced the LS1 coils and the coil harness.

And??? Nothing.?? Fuel flow and injector gross function verified.?? All sparks verified during cranking with a timing light.?? Tried a different CAS just for kicks.?? The engine is a little tight because it is new, compression is not spectacular cause the seals have not set, perhaps the apex seal little bits are still glued on..

Jump in here anytime.


You know? You are right, I just need to disconnect the alternator and keep cranking until it finally catches and gets a little bit of a break-in.????

This talk has been really helpful for me.

Dave Leonard
(the forever optimist)
Also going to switch to full synthetic 2-stroke oil without MMO.?? The new engine will never know how good it has it.??



On Thu, Aug 29, 2019, 10:18 P= M Matt Boiteau mattboiteau@gmail.com <flyrotary@= lancaironline.net> wrote:

Well ran into a little bit of a snag on my RX8 engine???.
While trying different things to cool down the oil, during high-speed taxi tests I managed to blow out the temporary clear level tube on my coolant expansion tank, which lead to pressure loss, which caused it to overheat. Managed to shut down near the hanger and get a water hose on the rads, but I feel the engine got baked underneath the fiberglass cowl. *Future note, need to come up with some flaps that open after shutdown or something, to let the heat escape out. Maybe even an electric fan that runs for 5 minutes after shutdown*

I know I blew some type of coolant gasket, but unsure if the irons are warped. Going to take apart next weekend. Just wanted to run by my list of mods, to see if I need to change anything or add/remove.

25hours, 99% ground testing
The iron plates were lapped and renitraded
Rotor housings were new and welded in P-Ports
RotaryAviation master kit (RA super seals)

Oil
~125psi at full throttle
20w50 VR1 high zinc
RX7 rear pressure regulator
2 washers under front pressure regulator
weber jet kit
thermal pellet


Coolant
1.3bar cap
ECU says ~27psi at full throttle, not sure I believe that yet. Lots of noise at full throttle on my pressure sensors (pic attached)
70/30 Zerex G-05

??

I???ll order the Atkins oring kit, supposedly their brown inner water jacket seals can handle a bit higher temps. https://www.atkinsrotary.co= m/store/04-11-Rx8-O-Ring-Kit-ARE317.html


- Matt Boiteau
--
Homepage:?? http://www.flyrotary.com/ Archive and UnSub:?? ??http://mail.lancaironline.net:81/lists/flyrotary/List.html=


=20
--000000000000277ae3059196f42b--