Hi Jeff. I’ve done lot’s of experimenting with cooling sys. Tough to
explain all this, but I’ll give it a try:
Pretty clear you saw 6 psi only because you took off with 3+ cups of air in
the system. If you’d taken off with 2 cups of air, then pressure would have been
9 psi. 1 cup, 14 psi. No air in system, then you would have seen rated cap
pressure (16 psi in your case).
Sorry to say, the pressure you see has no significant effect on cooling
efficiency (heat transfer). The next time you fly, since you’ve removed most of
that air, you will still see 210F. Just like before. There’s one huge exception
to that statement, that’s if you have air in sys that can’t move to a high point
out of the flow. In that case air in sys has huge negative effect. Causes local
boiling when it passes hot areas and inflates cooling temp.
You don’t have to fly to prove these concepts. Ground running at idle is
all that’s needed. Let’s assume all air is removed. Then letting engine warm up
to 180 F will result in rapid pressure rise to 16 psi (rated cap pressure).
Fluid will exit system. With 2 cups of air in sys, that same 180F will yield
slow rise in pressure to only 9 psi. No fluid will leave sys.
A good cooling design pretends air is stuck in block, so you add a path for
that air to rise out of the block coolant flow. This is called a dynamic bleed.
Air is automatically removed from engine coolant flow. Super low risk way to fly
as you no longer care if air is in system. It’s can’t affect cooling.
It’s a bit higher risk to fly without dynamic air bleed, you just make darn
sure you purge all air from block sys prior to flight. Applying vacuum to rad
cap is great way to remove air.
One of the ironies about cooling design is that air that resides above
engine flow is a safety asset. For example, your cap is highest point in sys and
you have 2 cups of air under cap. Big safety advantage simply because your
pressure gage is then a great predictor of how well your sys is doing. A leak
will be detected long before overheating. A bunch of other assets to this
design.
Conversely, air in engine flow has overwhelming negative affect. Temps soar
and risks boil over.
Clear as mud eh?
Fwiw
-al wick
Sent: Wednesday, May 06, 2015 4:54 AM
Subject: [FlyRotary] Re: Return to Flight
Dave,
I can’t argue with your adequate theory; I have that for my oil cooling system,
along with the temperature-controlled Mazda oil cooler, I never worry about oil
temperature.
It’s
the practical application of that theory to the radiator installation that has
plagued me from the beginning … after the next flight I’ll know where I stand
and if there’s still a problem, then radical change may have to be the
recipe.
Jeff
From: David Leonard
[mailto:flyrotary@lancaironline.net]
Sent: Tuesday, May 05, 2015 9:31
PM
Subject: Re: [FlyRotary] Re: Return to
Flight
I agree with Bobby, this may (hopefully) be the cause, but if
so it just means that you didn't design in an adequate way to fill the coolant
without trapping air. You would hate to have to do a coolant-prep flight
every time you wanted to drain and refill the coolant. (but not the end of the
world).
I originally designed my system like Ed's. Minimal drag
(just the 2 stock RV-6 inlets) but cooling was like you and Ed describe...
OK, but you always have to keep and eye on it and often reduce power or AOA in
order to keep coolant temps in check. Then I made a major change to
provide TONS of air to an adequately sized radiator. Since, I never
even think about cooling. Yes, I do probably burn a little more fuel but
it is well worth it to never worry about cooling again. Its not rocket
science. Adequate air to an adequate radiator equals adequate
cooling. Change adequate to plenty in that sentence and now your are
rocking!
On Mon, May 4, 2015 at 12:37 PM, Bobby J. Hughes <flyrotary@lancaironline.net> wrote:
Jeff,
Congratulations on getting back in the air. That ½ quart
of coolant may have been trapped air that purged during flight.
Bobby Hughes
N416AS-
RV10 223 hrs
From: Rotary motors in
aircraft [mailto:flyrotary@lancaironline.net]
Sent: Monday, May 04,
2015 7:53 AM
To: Rotary motors in aircraft
Subject:
[FlyRotary] Return to Flight
Yesterday 3-May,
my bird got airborne once again on its maiden flight after 2+ years
rebuilding. I had a friend test-pilot fly it while I was flight engineer
watching the gauges. Flight controls and rigging were reported to be good
and the engine performed flawlessly. The oil temperature was stable around
160F (Mazda oil cooler in series with a Fluidyne) but again the water
temperature was high reaching 210F by circuit height so we backed off the
throttle, did a touch and go with a 500’ circuit and parked it. One
unusual result was the cooling system pressure was only at 5-6 psi; with the
high temperature it should have been 15-16 psi. Removed the cowlings and
found no leaks of either oil or glycol. I checked the coolant level and it
was down, requiring 1/2 quart to top it up. I also looked at my pinched duct and
think it needs more pinching, so am already starting to modify that – hope to
get another test flight in before the weekend.
Jeff
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