Mailing List flyrotary@lancaironline.net Message #52804
From: Dennis Havarlah <clouduster@austin.rr.com>
Subject: Re: [FlyRotary] Re: FW: [FlyRotary] Ready to fly again
Date: Thu, 4 Nov 2010 10:45:09 -0500
To: Rotary motors in aircraft <flyrotary@lancaironline.net>
Here is a picture of my foam intake ramp placed in the bottom of the James rotary cowl using orange transparent tape and the second picture is a side view of one of the foam inserts.  I glued the foam pieces into the cowl and covered them with a thin layer of fiberglass.
 
Dennis Haverlah
----- Original Message -----
Sent: Sunday, October 31, 2010 10:06 PM
Subject: [FlyRotary] Re: FW: [FlyRotary] Ready to fly again

 

Dennis,

Could you please describe the “hump” a little better?  Are you talking about trying to turn the air in the plenum?  Pictures perhaps?

 

Bill B

 


From: Rotary motors in aircraft [mailto:flyrotary@lancaironline.net] On Behalf Of Dennis Havarlah
Sent: Sunday, October 31, 2010 10:30 PM
To: Rotary motors in aircraft
Subject: [FlyRotary] Re: FW: [FlyRotary] Ready to fly again

 

Chris & Terria

 

My Catto 76X88 prop for the Renesis has a maximum cord of 6 ".  If yours is wider I believe it is too big for the engine.  My static was 5730 rpm  on a  90 deg day.

 

When I first started flying the rotary (three years ago) I had oil and water cooling problems - I used a home made wind tunnel 2 inches wide inserted into the cowl and blew air into it with a squirrel cage blower from a home A/C unit.  I used a manometer on the back side of the radiator to measure air pressure as the air came through the radiator.  I found I needed a good hump in the lower part of the cowl inlet to deflect incoming air evenly through the oil and water radiators.  My radiators are side-by-side.

 

You might use a GPS to compare with the air speed gages to make sure they are in the ball park.

 

Dennis H.

 

RV-7A

Renesis

RD-1C

Catto 76X88

 

 

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