The single rotor engine is finally running again. 
Dynamically balanced and a new ignition system helped a lot. 
 
The prop is set to give around 6000RPM at WOT. The 
repeated result are:
 
RPM           
6000/min
 
Fuel flow      6.8 
gph
 
MAP            
27"
 
Mixture         14.6
 
EGT              
1700 F
 
Oil and water temperatures were stable at 160/140 
respectivly. 
 
The fuel flow would indicate 80hp at a BFSC of .5 . 
If this is anywhere close to what the engine produces, the predicted 110hp at 
7500RPM are feasible. Keep in mind that this is a 12A based engine. For a 13B 
based version it will be close to 150hp. 
 
I now will have to put all my efforts into putting 
the flyable engine together.
 
Richard 
Sohn
N2071U