From:
Rotary motors in aircraft [mailto:flyrotary@lancaironline.net] On Behalf Of Steve Brooks
Sent: Monday, December 11, 2006
6:25 AM
To: Rotary motors in aircraft
Subject: [FlyRotary] Great Flight
Yesterday, the weather was outstanding. A
little cool at 56 degrees, but sunny and no wind. It was very nice to
drive only 15 minutes to the airport, to take the plane up for a flight around
the area.
On the flight bringing it up to NC 2 weeks ago, I
thought that the engine was running a little rich, and after trying option 9 to
lean it up, it really didn’t change too much. Then, in a moment of sheer
brilliance, I decided to lean it a little more using mode 3. Still didn’t
change the mixture much, but I was happy with it, so I left it alone.
When I throttled back upon arrival, the mixture bottomed out, and the engine
stumbled pretty bad. After a quick rotation of the mixture control, and a
couple clicks on option 9, it was running good again, until I throttled back a
little more, and started the cycle all over again.
A couple of days later, I went to the airport and
decided at this point, my best option was to return to factory default, and
start over, which I did. After tuning it for 10 minutes or so, I figured
it was good enough for a flight.
After preflight and taxi, my oil temperature was at
140 degrees, but my coolant was still laying on the 100 degree peg. That
is quite different than normal. I waited for a few minutes until it
started to move, just to make sure that it was working. When I took off,
I pushed the throttle forward, and the engine roared to life. It really
roared to life, because it was running at about 8 lbs of boost. I backed
it down a little to 5 lbs, and it backfired once, but then ran
smoothly. After climb out to about 2000 feet, the water and oil
were only at 160 degrees, which was really a surprise. It was a little
cooler than normal, but the temperatures were running about 20 degrees cooler.
I flew for about 20 minutes, surveying my new flying
area, and just enjoying the view. I then decided to check out the tuning
and started lowering the power. I found several points where the mixture
was really lean, and I made adjustments (option 9 only) to get it where it
needed to be. I think that it probably tuned better now, than it ever has
been, so I’m not going to mess with it anymore.
Temperatures never did get above 160 degrees, which
makes me wonder if I had an air bubble in the cooling system that worked out
during, or after the long flight 2 weeks ago. Whatever it is, I like
it. I slowed up to 100 kits approaching the downwind, and made a perfect
approach and landing. After the decent and landing, temperatures were at
about 140 degrees, and the engine was running very good.
It’s very nice to can add fuel and fly, but I think
that before my next flight, I’ll pull the top cowling, and just give everything
a once over, to make sure that everything is still good. I’ll also
re-torque the prop.
Steve Brooks
Cozy MKIV N75CZ
Turbo Rotary – 48 hours and counting.