Mailing List flyrotary@lancaironline.net Message #34734
From: Tracy Crook <lors01@msn.com>
Subject: Re: [FlyRotary] Great Flight
Date: Mon, 11 Dec 2006 18:34:36 -0500
To: Rotary motors in aircraft <flyrotary@lancaironline.net>
Hi Steve, as you noticed,  fiddling with mode 3 while in-flight is risky since it changes the mixture at all throttle settings, not just the one you are currently using. 
 
 Mode 3 is only for initial ground tuning to get the injector flow rate in the ball park.  As noted in the instructions, Mode 3 should be set at high throttle with the mixture control at 12:00.   If you find that Mode 1 or 9 runs out of range and can't get the mixture correct at some setting,  re-evaluate the situation for a possible change to Mode 3 when safely on the ground.
 
Also note that it can take many pushes on the Store button in mode 9 to get full range of adjustment.   Just because the program knob is at max rich setting does not mean that pushing the button sets it at full rich in this mode.   Instructions give full details on this. 
 
BTW, I appreciate all the feedback I can get on how the EC2 works on a turbo setup since I have never tweaked on one myself.
 
Glad you are enjoying the plane at last!
 
Tracy
----- Original Message -----
Sent: Monday, December 11, 2006 9:24 AM
Subject: [FlyRotary] Great Flight

Yesterday, the weather was outstanding.  A little cool at 56 degrees, but sunny and no wind.  It was very nice to drive only 15 minutes to the airport, to take the plane up for a flight around the area.

 

On the flight bringing it up to NC 2 weeks ago, I thought that the engine was running a little rich, and after trying option 9 to lean it up, it really didn’t change too much.  Then, in a moment of sheer brilliance, I decided to lean it a little more using mode 3.  Still didn’t change the mixture much, but I was happy with it, so I left it alone.  When I throttled back upon arrival, the mixture bottomed out, and the engine stumbled pretty bad.  After a quick rotation of the mixture control, and a couple clicks on option 9, it was running good again, until I throttled back a little more, and started the cycle all over again.

 

A couple of days later, I went to the airport and decided at this point, my best option was to return to factory default, and start over, which I did.  After tuning it for 10 minutes or so, I figured it was good enough for a flight.

 

After preflight and taxi, my oil temperature was at 140 degrees, but my coolant was still laying on the 100 degree peg.  That is quite different than normal.  I waited for a few minutes until it started to move, just to make sure that it was working.  When I took off, I pushed the throttle forward, and the engine roared to life.  It really roared to life, because it was running at about 8 lbs of boost.  I backed it down a little to 5 lbs, and it backfired once, but then ran smoothly.   After climb out to about 2000 feet, the water and oil were only at 160 degrees, which was really a surprise.  It was a little cooler than normal, but the temperatures were running about 20 degrees cooler.

 

I flew for about 20 minutes, surveying my new flying area, and just enjoying the view.  I then decided to check out the tuning and started lowering the power.  I found several points where the mixture was really lean, and I made adjustments (option 9 only) to get it where it needed to be.  I think that it probably tuned better now, than it ever has been, so I’m not going to mess with it anymore.

 

Temperatures never did get above 160 degrees, which makes me wonder if I had an air bubble in the cooling system that worked out during, or after the long flight 2 weeks ago.  Whatever it is, I like it.  I slowed up to 100 kits approaching the downwind, and made a perfect approach and landing.  After the decent and landing, temperatures were at about 140 degrees, and the engine was running very good.

 

It’s very nice to can add fuel and fly, but I think that before my next flight, I’ll pull the top cowling, and just give everything a once over, to make sure that everything is still good.  I’ll also re-torque the prop. 

 

Steve Brooks

Cozy MKIV N75CZ

Turbo Rotary – 48 hours and counting.

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