Yesterday, the weather was outstanding. A little cool at 56 degrees, but sunny and no wind. It was very nice to drive only 15
minutes to the airport, to take the plane up for a flight around the area.
On the flight bringing it up to NC 2 weeks ago, I thought that the
engine was running a little rich, and after trying option 9 to lean it up, it
really didn’t change too much.
Then, in a moment of sheer brilliance, I decided to lean it a little
more using mode 3. Still didn’t
change the mixture much, but I was happy with it, so I left it alone. When I throttled back upon arrival, the
mixture bottomed out, and the engine stumbled pretty bad. After a quick rotation of the mixture
control, and a couple clicks on option 9, it was running good again, until I
throttled back a little more, and started the cycle all over again.
A couple of days later, I went to the airport and decided at this point,
my best option was to return to factory default, and start over, which I
did. After tuning it for 10
minutes or so, I figured it was good enough for a flight.
After preflight and taxi, my oil temperature was at 140 degrees, but my
coolant was still laying on the 100 degree peg. That is quite different than normal. I waited for a few minutes until it
started to move, just to make sure that it was working. When I took off, I pushed the throttle
forward, and the engine roared to life.
It really roared to life, because it was running at about 8 lbs of
boost. I backed it down a little
to 5 lbs, and it backfired once, but then ran smoothly. After climb out to about 2000
feet, the water and oil were only at 160 degrees, which was really a surprise. It was a little cooler than normal, but
the temperatures were running about 20 degrees cooler.
I flew for about 20 minutes, surveying my new flying area, and just
enjoying the view. I then decided
to check out the tuning and started lowering the power. I found several points where the
mixture was really lean, and I made adjustments (option 9 only) to get it where
it needed to be. I think that it
probably tuned better now, than it ever has been, so I’m not going to mess with
it anymore.
Temperatures never did get above 160 degrees, which makes me wonder if I
had an air bubble in the cooling system that worked out during, or after the
long flight 2 weeks ago. Whatever
it is, I like it. I slowed up to
100 kits approaching the downwind, and made a perfect approach and
landing. After the decent and
landing, temperatures were at about 140 degrees, and the engine was running
very good.
It’s very nice to can add fuel and fly, but I think that before my next
flight, I’ll pull the top cowling, and just give everything a once over, to
make sure that everything is still good.
I’ll also re-torque the prop.
Steve Brooks
Cozy MKIV N75CZ
Turbo Rotary – 48 hours and counting.