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That's
possible. I'm not sure how much it sagged, but it seemed
significant. May have only been a couple hundred RPM's though. At
least while still on the ground, it didn't have the same pucker effect that it
would have a little later.
I was
really impressed with the engine performance, just before it sagged. It
really put me back in the seat on the takeoff roll. If I had pushed it to
full throttle, I'd probably been really impressed. Of course, I'd been
airborne earlier, so it's a good thing that I didn't
Steve
I get the spark plug sag after about 50-100 hours on a
set of leading plugs. It usually happens the first time after takeoff and I'm
a few hundred feet in the air, but it's never that "drastic", just 100-200 RPM
drop. It does get your attention!
Kelly Troyer wrote:
Steve,
May be the famous "Spark Plug Sag" as reported by Tracy
and Ed !!
-- Kelly Troyer Dyke
Delta/13B/RD1C/EC2
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Original message from "Steve Brooks" <prvt_pilot@yahoo.com>:
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> I went to South Carolina Thursday to
replace the fuel regulator, and do some > flying. I replaced the
regulator, and ran the engine some on Thursday, but > no flying
because it was getting dark. > > On Saturday, I went to fly,
and had some trouble getting it to stay running > due to the cold
temperatures. I probably didn't keep it rich enough, long > enough.
I taxied out to the far end of the runway (5000'), and took the >
runway for take off. > > As I accelerated to about 90 kts, I
was just rotating when to power dropped > substantially. I cut the
throttle, and aborted the takeoff. > > I don't know exactly
what caused the sag. I pulled the throttle all the way > back
during the aborted takeoff, and the engine died. I have my idle stop
> set a little low (400 RPM's), and usually don't pull it all the
way off, but > even when I do, it has never died. > >
I restarted it, and ran the power up to about 4000, and it seemed OK.
> > Another issue with my right main wheel bearing prevented
me from making any > more high speed runs. The right wheel has been
making noise, and I was > trying to resolve it with the mfg, but
during the aborted take off, it > really made allot of noise, and
also vibrated pretty good at one speed, so I > decided that I
better get that fixed before doing any more flying. > > I
changed the fuel regulator, so I guess that it could have been some air
> still in the fuel line, but the engine had probably run for at
least 10 > minutes prior to the take off roll. It also could have
been some water, > though I've never found any to date during
preflight. The engine was > running at 5 lbs of boost and abo ut
5000 RPM's. It was about 45 degrees, > and the plane was
accelerating very strong prior to the power loss. I don't > know if
it would have picked back up, but I was glad that it didn't happen 5
> seconds later. > > Steve Brooks > >
> >> Homepage: http://www.flyrotary.com/ >
>> Archive: http://lancaironline.net/lists/flyrotary/List.html
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