May 26, 2013 events of
Lancair
N471LA Nose gear failure at F45
Submitted by Paul A.
Hershorin
On Sunday morning at about 9:30 a.m.
my
wife Pat and I, after doing our preflight inspection and engine checks, took
off from F45 (North Palm Beach Air Park) to fly to Florida Keys Marathon (MTH)
for lunch. Upon lift off we had 22
gallons of fuel on board for a 40 minute flight. We climbed to 8,500 feet VFR, I set up the
plane on a fuel burn of 8.4 gallons per hour and we indicated 240 miles per
hour. It was a beautiful flight without
any problems. We landed, parked the
plane and went into the FBO signed in and went to Burdines for lunch which was
most enjoyable.
After lunch, we returned to the FBO,
visited
the EAA museum and then Pat rested in the FBO while I moved the plane to the
fuel pump. To move the plane to the gas pump I used my tow bar. I did not see any oil or hydraulic fluid
on
the ground by the nose wheel or on the nose strut at this time. The
plane took 26.35 gallons of fuel and then I did my preflight inspection. There were not any preflight problems. We taxied to runway 07,
did the engine
checks, announced that we were taking active runway 07 and will be departing to
the north. Upon lift off I raised the
gear lever and flap switch and immediately noticed no gear lights showing up or
down. I told my wife there was a
problem—no lights and the plane was not accelerating—I could tell that the gear
had not retracted. I announced to MTH
that we had no lights indicating the position of the landing gear and that I
was going to circle and do a low pass over runway 07—could someone tell me the
position of the gear. First pass I was
told that it was “UP”, however, with the drag on the plane I said that I would
make a second pass—this time there was a helicopter watching that said the gear
was “down” I tried to recycle the gear
without any luck. I told my wife that we
would fly to our home base F45 along the coast.
About 15 or 20 miles out of MTH we had
a
warning light telling us that the “volts”
was in the yellow range—my hydraulic pump light indicator was on so I
pulled the 50amp breaker—the “volts” went from 9 back up to 13-14. It was a slow flight at 143 kts. at
2,000
feet looking out for many planes and staying out of Miami and then Ft
Lauderdale air space.
When we reached Boca I
called Palm Beach tower and told them the problem that I was having and asked
if I could do a tower fly by and if they
could tell if the gear was locked down.
On the first pass I was too low for the tower to be able to tell if the
gear was locked in or not so I was asked to come around again but higher this
time. I came around at about 250 feet
and the tower said that they thought it may be locked in place but they had no
way of knowing. I asked to go to my home
base at F45 and they vectored me on course.
Here is the problem—to
lock in the main gear I did side movers to catch the wind on the gear doors
that are attached to the gear, this locked them in, however the nose gear free
falls from the up position being pushed by a gas strut—no way of knowing if it
was in position or not. I announced a
right hand down wind for runway 08R at F45, announced a right base and then
final 08R full stop—somewhere in the discussion or Palm Beach tower announced
to F45 I was having gear problems—on final I told Pat to remove her glasses in
case she might hit the dash, said that on touchdown I was going to pull the
fuel all the way out, turn off the ignition and three master switches which I
did—landed on the mains and held it off as long as I could and then it settled
on the props shattering all three blades and the plane came to a stop a 1,000
feet down the runway. Pat and I looked
at each other, I climbed out of the plane and saw people running from the FBO
and individuals on golf carts coming to our aid, I helped Pat out with
bystander help—the sheriff dept. arrived in two to three minutes and the fire
dept arrived in about 10 to 15 minutes.
Neither Pat or I were hurt, in fact it was a very smooth landing and
stop.
A fork truck was
brought out and I connected a tow rope to two blades of the propeller, the fork
lift lifted the nose of the plane and we pulled the nose gear into position and
strapped it to the two bottom propeller blades pulling the gear forward. The FBO sent out their
airplane tow and they
towed the plane to my hangar. While, waiting for the plane to be raised the
sheriff did his report, fire department did their report and I received a call
from the FAA stating that it was “OK” to move the plane from the runway and I
would be contacted this week by the FAA.
Upon inspection of the
nose gear by an IA, A&P it was found that the nose gear door hydraulic hose
fitting, aluminum, sheared off at the actuator.
This must have happened upon lift off when I moved the gear switch to
retract the landing gear and pumped all the hydraulic fluid overboard and
released the load on the nose gear. I
tried many maneuvers, but could not get the nose gear to lock in.
Once again, I want to
state that neither Pat nor I were injured and want to thank all the individuals
from MTH to F45 for their assistance and help.
Submitted by Paul A.
Hershorin 5/29/13