I thought I would share the solution to my boost control problem
which included a runaway over boost at takeoff and a wondering non-controlled
boost in level, climb and descent cruise flight.
I found through testing the wastegate did not have the capacity
to bypass enough exhaust and the turbos were therefore uncontrollable. Gary at
Main Turbo out of California was a huge help and found a different wastegate
with the same footprint but a larger ID. The new part arrived today, was
high speed taxi tested and then flown. The two hour flight was perfect
and the problem seems to be solved.
I must point out I have changed several parts in the turbo
system including custom intercoolers, custom tailpipes, removal of the tailpipe
restrictor and my own sonic nozzles. However, the sonic nozzles are made
to the Piper Mirage inside dimensions. I also have the large Mirage
compressors, 8.5 to 1 CR and an experimental camshaft. I am now adding a
larger ID wastegate to the list.
Craig Berland
N7VG