X-Virus-Scanned: clean according to Sophos on Logan.com Return-Path: Sender: To: lml@lancaironline.net Date: Thu, 04 Sep 2008 11:33:51 -0400 Message-ID: X-Original-Return-Path: Received: from asp-3.reflexion.net ([205.237.99.178] verified) by logan.com (CommuniGate Pro SMTP 5.2.7) with SMTP id 3113966 for lml@lancaironline.net; Thu, 04 Sep 2008 10:39:41 -0400 Received-SPF: none receiver=logan.com; client-ip=205.237.99.178; envelope-from=cberland@systems3.net Received: (qmail 9158 invoked from network); 4 Sep 2008 14:39:03 -0000 Received: from unknown (HELO asp-3.reflexion.net) (127.0.0.1) by 0 (rfx-qmail) with SMTP; 4 Sep 2008 14:39:03 -0000 Received: by asp-3.reflexion.net (Reflexion email security v5.50.2) with SMTP; Thu, 04 Sep 2008 10:39:03 -0400 (EDT) Received: (qmail 9068 invoked from network); 4 Sep 2008 14:39:02 -0000 Received: from unknown (HELO systems3.net) (98.172.79.178) by 0 (rfx-qmail) with SMTP; 4 Sep 2008 14:39:02 -0000 Content-class: urn:content-classes:message MIME-Version: 1.0 Content-Type: multipart/alternative; boundary="----_=_NextPart_001_01C90E9B.F8E3CFEB" X-MimeOLE: Produced By Microsoft Exchange V6.5 Subject: Legacy 199L X-Original-Date: Thu, 4 Sep 2008 07:39:00 -0700 X-Original-Message-ID: <87C33F695961494D886EB3B6C8A47651538096@s3server.Systems3.local> X-MS-Has-Attach: X-MS-TNEF-Correlator: Thread-Topic: Legacy 199L Thread-Index: AckKU2aODaxPl96oQNqar3C6D67GbgERbjEA From: "Craig Berland" X-Original-To: "Lancair Mail List" This is a multi-part message in MIME format. ------_=_NextPart_001_01C90E9B.F8E3CFEB Content-Type: text/plain; charset="US-ASCII" Content-Transfer-Encoding: quoted-printable I thought some may be interested in the actual events regarding 199L. =20 The engine blew up (literally) in 199L on the way back from EAA Goldenwest. Fortunately it was approximately 10 miles south of the Bend airport and the pilot deadsticked it there. I believe the engine over sped due to oil pressure loss. This I'm not 100% sure of as I was told this over the phone and my memory isn't what it should be. =20 The pilot didn't have quite enough altitude to make the overrun and landed around 200' short of it. Unfortunately, there was a ditch across the end of the overrun which took the main gear forks and tires off. He was able to wheelbarrel the aircraft on its nose gear across the overrun, through the runway lights and onto the runway until the plane lost lift and the aircraft settled on the main gear struts and tail. He lost directional control at that time and the aircraft eventually slid off the right side of the runway a bit. 199L is repaired and up and flying. Four hours of test flying have been put on a new engine and repaired airframe and instruction was done in it last week. There was no structural damage to the fuselage. Hope this helps. =20 The pilot is a very good friend and the information came directly from him. If ever a similar misfortune falls my way, I pray I have similar skills and thus a similar outcome. =20 Craig Berland =20 ------_=_NextPart_001_01C90E9B.F8E3CFEB Content-Type: text/html; charset="US-ASCII" Content-Transfer-Encoding: quoted-printable

I thought some may be interested in the actual events regarding = 199L.

 

=

The engine blew up (literally) in 199L on the way back from EAA Goldenwest.  Fortunately it was approximately 10 miles south of the Bend airport and = the pilot deadsticked it there.  I believe the engine over sped due to = oil pressure loss.  This I’m not 100% sure of as I was told this = over the phone and my memory isn’t what it should = be.

 

=

The pilot didn't have quite enough altitude to make the overrun and landed around = 200' short of it.  Unfortunately, there was a ditch across the end of = the overrun which took the main gear forks and tires off.  He was able = to wheelbarrel the aircraft on its nose = gear across the overrun, through the runway lights and onto the runway until = the plane lost lift and the aircraft settled on the main gear struts and tail.  He lost directional control at that time and the aircraft eventually slid off the right side of the runway a bit.  199L is = repaired and up and flying.  Four hours of test flying have been put on a = new engine and repaired airframe and instruction was done in it last = week.  There was no structural damage to the fuselage.  Hope this = helps.

 

=

The pilot is a very good friend and the information came directly from him.  = If ever a similar misfortune falls my way, I pray I have similar skills and thus = a similar outcome.

 

=

Craig Berland

 

=



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