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Yes, you are correct, Bill. I used a flow rate found in "Maximum
Performance" recommended for a turbocharger, I think it was a minimum of
0.5 gpm and I rounded it up to 1 gpm just to be on the safe side.
Ed
Ed Anderson
RV-6A N494BW Rotary Powered
Matthews, NC
----- Original Message -----
From: "William" <wschertz@ispwest.com>
To: "Rotary motors in aircraft" <flyrotary@lancaironline.net>
Sent: Sunday, June 13, 2004 10:52 PM
Subject: [FlyRotary] Re: Pressure Reduction Was Re: [FlyRotary] Re: Some
Taxi testing today. With oil leak.
> That would clearly have to be a function of flow rate, wouldn't it?
> Bill Schertz
> KIS Cruiser # 4045
> ----- Original Message -----
> From: "Ed Anderson" <eanderson@carolina.rr.com>
> To: "Rotary motors in aircraft" <flyrotary@lancaironline.net>
> Sent: Sunday, June 13, 2004 10:55 AM
> Subject: [FlyRotary] Pressure Reduction Was Re: [FlyRotary] Re: Some Taxi
> testing today. With oil leak.
>
>
> > Dave, a calculator I found on the Web indicated that with oil going from
a
> > 3/8" dia (AN-6) through a 1/8" orifice would reduce the pressure by
approx
> > 40 psi. So if your engine is putting out 70-80 psi that would bring it
> down
> > to the 30-40psi range which should be acceptable.
> >
> > Ed
> >
> > Ed Anderson
> > RV-6A N494BW Rotary Powered
> > Matthews, NC
> >
> >
> >
> >
> > >> Homepage: http://www.flyrotary.com/
> > >> Archive: http://lancaironline.net/lists/flyrotary/List.html
>
>
> >> Homepage: http://www.flyrotary.com/
> >> Archive: http://lancaironline.net/lists/flyrotary/List.html
>
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