Here's my latest trip report and an illustration of the difficulty of troubleshooting at a distance.
A couple of years ago I agreed to develop a GM LS-1 - LS-7 V8 engine controller based on the EC2. Part of the agreement was that the developer would do extensive testing, report all test results and get all problems resolved prior to any customer deliveries. The developer reported that the first unit worked perfectly and began customer deliveries. "Damn, I'm Good!" I (prematurely) said to myself.
Soon, I began receiving calls from the developer's customers. They were having various difficulties with no identifiable pattern based on their descriptions. When I had them return the units for testing, no problem was found with the controller in all but rare cases. In talking with the developer, I asked if they had seen any of these problems in their testing. Over the course of many of these conversations it became clear that no real testing had been done other than to start the engine and idle it on a test stand with no load. I'd been "had" and would now be forced to deal with dozens of individual builders with unknown engine skills to resolve their problems or watch my reputation go down in flames. Worst of all, I now had no confidence that the basic software design was any good since it was essentially untested other than on my engine simulator on the bench (I have no GM V8 to test on).
After more than a year of email exchanges with many of the developers customers, only a few were successful in getting reasonable results but all of them assured me that the installation instructions had been followed to the letter. I had no choice but to look at one first hand.
With the RV-4 packed with everything I thought I'd need, I departed for Savanna Georgia where the closest installation was located. Beautiful CAVU day with the Renesis humming sweetly. Set fuel burn at 6.5 GPH, tune XM radio to desired music (40's music on this day), follow the course line to SAV on the Garmin with no weather in sight. Only a few Restricted areas to dodge south of the airport. Marvellous flight, the best possible use of 8.5 gallons of 87 octane regular (with 10% Ethanol) on the 200 mile flight.
As expected, I saw how rusty I was in dealing with Class C airports. Get ATIS, contact approach control, get squawk code, carefully hold instructed altitude (never easy in an RV when tuning radios, etc), follow vectors for approach , switch to tower & contact, get clearance to land. Had a rare perfect cross wind landing on concrete then plead ignorance to tower and beg for progressive taxi to the desired FBO, contact ground control find a parking spot then finally shut down. Really complicated compared to my normal straight in approach to the grass at Shady Bend. I guess you'd eventually get used to it.
Checked out the builders plane which was a beautiful RV-10. It was equipped with virtually everything (including airconditioning) you can put in an airplane, not to mention the LS-2 V8 with supercharger. All this added over 300 pounds above the heaviest IO - 540 powered RV-10. If flown solo, a minimum of 100 pounds of ballast was to be carried in the back seats to maintain CG at forward limit.
Anyway, below are my notes from the troubleshooting session that followed. I have to point out that in over a year of email correspondence I never got any report that remotely resembled the symptoms I observed except for the high throttle miss. OK, I feel better now after bitching about it. Such are the perils of long distance troubleshooting.
Tracy Crook
On 11-16-08 made trip to Savanna GA
(KSAV) to check builder EC2 installation and found the following.
1. EC2 was not grounded
to airframe close to EC2 per instructions.
Had 2 ground wires attached but they were longer than acceptable and went to a
noisy destination on electrical system.
The case was electrically isolated from ground by foam tape between it
and the mounting bracket, contrary to instructions. Could not sync up EM3 due to electrical noise induced communications
errors. Even without EM2 adapter in
line, unit would not consistently enter test modes (1 or 8) also due to noise. Unit also showed a couple of instances where
map table was programmed spontaneously due to noise. Installing
a short wire to airframe eliminated these symptoms.
2. At one point in
testing, found that cylinder 5 and 8 were not firing. This turned out to be due to Blue Mountain
tach connection to the 5 & 8 coil driver which is not recommended. This shunted the signal to ground when the
Bluemountain was not on.
3. The crank signal
was measured with an oscilloscope and found to be of low amplitude and was
modulated by off center trigger wheel.
The signal amplitude varied by as much as 30% (average) and 100% after the sync gap
initial pulse. Even with the engine at
highest RPM tested, the CAS signal amplitude was only 2.4 V P-P at the highest
point. Note, tach on plane was way out of calibration and
measured prop rpm instead of engine rpm, (not recommended). I estimate that the engine rpm was ~ 2400 - 3000
RPM. This is much less than the sample
Electromotive sensor evaluated here
(Builder's spare) which gave at
least 12 V P – P at only 1200 RPM. I
think this is due to the mounting of the sensor offset axially by approximately
.22". This must be corrected.
4. The EC2 flow rate
was found set to maximum and even this was not enough to get enough fuel flow
at ~ 25% of available manifold pressure.
When higher manifold pressures
were eventually tested, the mixture went rich and was well within range of the
available flow rate. I determined that
the dynamic range setting of the EC2 was way too high for the LS-2 injectors and this particular
engine – prop combination. This is why the customer was always setting the
flow rate to the inappropriate max setting because they were setting Mode 3 at
too low a manifold pressure setting, probably due to the rough running at
higher throttle. The dynamic range was adjusted using Mode 2
and the mixture could then be well adjusted at all tested throttle settings
when using the default inj. flow rate.
Must change the default dynamic range setting for LS-1/2 type engines
and clarify the tuning procedure to caution for this situation.
5. The one remaining
problem that remained in testing this installation was an occasional miss at
higher throttle settings. I think this
is due to the low amplitude and modulation of the crank angle signal causing the EC2 to loose synchronization. If the amplitude were higher, the modulation
due to non concentricity would not be a problem but the combination of the two
is unacceptable. It is expected that moving
the sensors axially so that they are centered on the trigger wheel and making sure that the sensor gap is close
to .020" will eliminate this
problem.
Action Plan:
Configure an EC2 closer to the required injector flow rate and dynamic
range for this engine so that the builder will have a much simpler job setting
the EC2 up. See if I can make the EC2
crank sensor less susceptible to crank sensor signal modulation at even low
signal levels. Even if possible, this
does NOT eliminate the need to remedy the crank sensor mounting misalignment. Send
this configured controller to builder to swap out his current EC2 controller.
Builder Changes Required:
1. At minimum,
install a short (< 12") wire (16 ga or heavier) to airframe ground near the
EC2 to the EC2 ground stud. If
possible, the mounting method for the EC2 should directly ground the EC2 case
to the airframe. This is the preferred mounting
method for the EC2 but the short ground wire should still be installed.
2. The crank sensor
mount must be modified in order to have the crank sensor centered axially on
the trigger wheel. Crank sensor gap
should be set at .020" and should not vary by more than .003" around the
circumference of the trigger wheel. If
gap varies more than this, I recommend that the wheel be removed and machined
in a lathe in order to take the high points off the teeth (equalize the gap
around the wheel).
3. I strongly suggest
that the connection to the cylinder 5/8 coil trigger from the Bluemountain EFIS
be removed. The injector driver on Pin
17 of the EC2 is a suggested replacement.
Check with Bluemountain if this is a workable solution.
4. When the replacement EC2 is received and after doing
the above changes, carefully follow the suggested tuning procedure in the EC2 installation
guide. Adjust both the Mode 3 and Mode
2 setting before doing any adjustments in Mode 1. Report
results to me at RWS.
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