Return-Path: Sender: (Marvin Kaye) To: flyrotary Date: Mon, 20 Oct 2003 22:45:48 -0400 Message-ID: X-Original-Return-Path: Received: from [24.93.67.84] (HELO ms-smtp-03-eri0.southeast.rr.com) by logan.com (CommuniGate Pro SMTP 4.1.5) with ESMTP id 2642844 for flyrotary@lancaironline.net; Sun, 19 Oct 2003 18:30:27 -0400 Received: from o7y6b5 (clt78-020.carolina.rr.com [24.93.78.20]) by ms-smtp-03-eri0.southeast.rr.com (8.12.10/8.12.7) with SMTP id h9JMUPuf009214 for ; Sun, 19 Oct 2003 18:30:26 -0400 (EDT) X-Original-Message-ID: <003d01c39690$5d06f560$1702a8c0@WorkGroup> From: "Ed Anderson" X-Original-To: "flyrotary" Subject: Sigh! Another engine out Glide! X-Original-Date: Sun, 19 Oct 2003 18:28:47 -0400 MIME-Version: 1.0 Content-Type: text/plain; charset="iso-8859-1" Content-Transfer-Encoding: 7bit X-Priority: 3 X-MSMail-Priority: Normal X-Mailer: Microsoft Outlook Express 6.00.2800.1106 X-MIMEOLE: Produced By Microsoft MimeOLE V6.00.2800.1106 I truly appreciate all the supporting e mails consoling me about no longer being on the rotaryeng list, don't know what I would have done without it {:>). Actually, I was so concerned I went flying today, beautiful day with clear skies and moderate temperatures. Also wanted to check out that the gearbox Tracy had shipped back was properly installed with no oil leaks, etc., before I flew down to Shady Bend this coming weekend. This was the first flight since Tracy fixed the gear box that my flaking nickel plating almost did in. I had been thinking had I gotten airborne and had that gearbox seize up - it would not have been nice. So as you might imagine I was keenly attuned to anything unusual as I took off on this first flight after reinstalling the gearbox. Also wanted to check that my 33% decrease in radiator duct inlet area was still cooling adequately. After flying approx 20 minutes I was turning over a small airport to head back home and check under the cowl to make certain no oil leaks, when suddenly there was a terrific racket and a vibration through the airframe. I hastily scanned all my engine instruments - fuel pressure OK, Water oil temps OK, oil pressure OK, - wait, was it fluctuating a bit?. The engine was still turning, but for how long? Was there more nickel plating in some place I had failed to notice, was the gear box seizing, was the engine fixing to seize. Those and more thoughts took about 9/10ths of a second to race through my head (well, maybe a bit longer). My incisive conclusion was that "something" was wrong with the engine and/or gearbox. Since the only thing I had recently messed with was the gearbox and the oil supply they were the prime suspects - I had images of the engine seizing (yeah I know the oil pressure said OK, but it appeared to be fluctuating a bit - you have to be there) and possibly throwing a prop. Also if an oil problem, I really didn't want to fry the bearings of the engine. Releasing my grip on the seat cushion, I leaned over and flicked off the fuel injectors. Well that did stop the noise and vibration, as well as the prop which slowed down and stopped - no surprise there! I've see that before! Altitude was 4000 MSL. Only the "whoosh" of air over the canopy and the zzzzzz of the fuel pump which I decided to leave on should I decide to relight the fire. So I raised the nose for best glide speed and started down for the airport. Hey, this is the second time and this time I even managed to get off a few radio calls to the airport Unicom. Just advised them of some engine difficulties and that I would be ahem....making a "precautionary" landing on 17 in a few minutes {:>). Once again, I confirmed that best glide was 87 MPH which gave me 650-750 fpm rate of descent in my RV-6A. Came over the down wind end (at least that was different than the first time), checked my altimeter and confirmed what my eyeball said. Dumped full flaps as I do come in a bit on the high side normally (and especially when the fan is stopped), did some slipping and "S" turns to bleed off altitude and made a nice landing and rolled off the runway at the first taxi way. A group of the local airport crowd came up and pulled me back to the FBO area. Well, to make a long story shorter, nothing wrong with the engine or gear box. My *&#^% pilot side muffler pipe (I have one on each side underneath) had backed out of its header tube and the terrific noise I heard was simply 120 DB exhaust right under my feet. Can actually feel the exhaust impulse on the floor board which accounted for the vibration I had felt. But, I was so attuned to a gearbox/engine scenario that it never occurred to me that it was simple the exhaust - so again a bit embarrassing, but not as much as the failure to switch fuel tanks that first time. Besides, I don't think I really wanted that hot exhaust blowing straight out of the header back on that thin aluminum bottom. So, found out that a pin that I use to keep the two tubes together had apparently failed and the clamp itself couldn't hold the tubes together. The FBO was serving free hamburgers, so enjoy meeting another group of hangar bums and had a great lunch. Fixed the exhaust and had an uneventful flight home. So my "glider" time is now up to about 15 minutes and it was a bit less thrilling (if you believe that {:>)) than the first time over broken overcast. Like I say, if its going to happen - it WILL happen to me - well, I admit - I did intentionally shut off the engine this time to preclude damage and to keep it ready should I find my gliding eyeball was inaccurate and needed a power boost toward the end of the glide. Just another day of adventure in rotary land with Ed Anderson. Ed Anderson RV-6A N494BW Rotary Powered Matthews, NC eanderson@carolina.rr.com