Well I can breathe again!
On Memorial Day, N821GL took to the sky. What an incredible
experience!
Water temp got up to 220 and oil peaked at 208 so there is
room for improvement. I was throttled back most of the flight so a little more
speed might help. I did push it up to 6200 and 140 MPH for a short bit. Water pressure
peaked at 23 psi, so I cut the flight short.
On post flight I found that water was being pushed past the cap
on the radiator. And the can muffler radiates WAY to much heat. So it's
on to rev B. Closing the radiator cap up and constructing a new exhaust system.
I will post some pictures soon. Thanks to all that have
paved the way!
Thanks,
Jason Hutchison