12-31-05
Made the first
attempt to crank the engine today.
This turned out to be a good news/ bad news event. The good news is that it fired up
instantly, and everything seems to work.
The bad news is that it’s rough as a cob :-0
It would
appear that my worst fears about the torque reversals with the RD-1C drive have
come true. I didn’t notice the rpm,
but the engine barely made it over the speed the starter turns it. In fact, the starter stayed engaged a
couple times, because the engine didn’t accelerate enough to push the gear
back. Did I mention that’s it’s
rough :-) It just shook the living
crap out of the plane, but the engine mounts work well. The main gear of the
plane was actually jumping slightly off the ground. Good thing I was sitting in the plane,
or it really might have been interesting.
While the
engine was running, no amount of throttle changes anything. It’s simply impossible for the engine to
accelerate out of this mode.
BTW, this is EXACTLY how the 912S used to behave on this plane. If you didn’t crank the engine with
enough throttle opening, it would get stuck in the gearbox shaking mode, and the
best thing you could do was shut it down, and try again. Rotax came out with a “slipper clutch” to eliminate the problem
on the 912S.
Next step will
be to remove the prop, and try it that way. Eliminating the rotational mass of the
prop should make it better, if not eliminate the problem altogether. If that works OK, then I may have to try
a different hardness of rubber dampeners on the redrive thrust plate. If it doesn’t work, then I’ll likely
pull the drive itself off, and try it that way.
1-1-05
Much better
today. It appears that some dumbass
marked my pulley wrong :-)
Tracy says to put a new mark on the
pulley that's 35 degrees BTDC, and set the static timing to that. The
RB pulley has 4 equally spaced marks on it- 10 ATDC, TDC, 10 BTDC, and 20
BTDC. Realizing that these are 10 degrees apart, I measured the
distance, and then figured out what one and a half times that distance would
be. This new distance would be 15 degrees, and if I put it beyond the 20
BTDC, I'd be at 35 BTDC. Unfortunately, when you have the pulley turned
around backwards on the workbench, and put the new mark on the OTHER side
of the existing marks, it becomes 25 ATDC. When I set the static
timing, I set it to my new mark, which I "knew" was right, so the timing
was retarded by 60 degrees. Amazing it ran at
all.
The good news
is that it runs much better now, even with the prop (didn't try without
it). There is still going to be a resonance issue with the redrive I
believe, as there are a couple RPM's that go into the same rattle mode that I
used to get around 1100 RPM on the 13B. The worst was around 2400 RPM, and
it also seemed rough around 3000, but not as much rattling. I didn't run
over about 4000 rpm, or more than a few minutes, since I suspected I still had
a bit of an oil leak, and didn't want to make too much of a mess.
There was oil
leaking at the fitting on top of the front housing, which I use to feed the
redrive. This is really a metric
fitting, but 1/8 NPT seems to fit well.
I ended up removing the fitting, and installing a new one, with some
miracle gray RTV for good measure.
Unfortunately, it leaked plenty during my few minutes of running. I
had the plane tied to the wheel of the company van, and it is completely covered
in oil. I do mean the whole van,
not just the wheel :-) I bet it's really only a half pint or so,
but it sure got spread around by the prop.
I also had an
odd case where the A controller seemed dead. The injectors wouldn’t click when I
pushed the set button, and the engine wouldn’t fire. The B controller worked normally, but
switching to A while running killed the engine dead. After I turned everything off, checked for leaks and such, then turned
it all back on again, the A controller seemed to be working fine. It’s now as if there’s no problem at
all. There's a long time before I could ever consider flying
the plane, so I'll just watch to see if this returns.
I need to
finish eliminating the leaks, then run it enough to purge any air from the
cooling system, and verify that all is well as far as cooling goes. At that point, I can give auto tune a
try, and then see if I can make some sense out of the torque reversal induced
vibrations.