Return-Path: Received: from chntva1-smrly1.gtei.net ([128.11.152.196]) by ns1.olsusa.com (Post.Office MTA v3.5.3 release 223 ID# 0-64832U3500L350S0V35) with ESMTP id com for ; Mon, 11 Sep 2000 10:01:45 -0400 Received: from molexinc-cp.molex.com (molexinc-cp.molex.com [204.167.149.71]) by chntva1-smrly1.gtei.net (Postfix) with SMTP id 0EF5C45F1 for ; Mon, 11 Sep 2000 14:05:51 +0000 (GMT) Received: from ccMail by smtp2.molex.com (IMA Internet Exchange 3.0 Enterprise) id 000C030E; Mon, 11 Sep 2000 09:03:19 +0100 Date: Mon, 11 Sep 2000 09:56:47 +0100 Message-ID: <000C030E.CE21031@molex.com> From: edechazal@molex.com Subject: First Flight of N361DC To: lancair.list@olsusa.com (Lancair) X-Mailing-List: lancair.list@olsusa.com Reply-To: lancair.list@olsusa.com Mime-Version: 1.0 <<<<<<<<<<<<<<<<--->>>>>>>>>>>>>>>> << Lancair Builders' Mail List >> <<<<<<<<<<<<<<<<--->>>>>>>>>>>>>>>> >> N361DC (my lancair 360) flew for the first time Saturday, September 9, 2000 at 10:50 am from Romeo airport (D98) in Michigan at the capable hands of Mike Dehate. What a day! I have a full report that Marv Kaye has asked be placed in the upcoming issue of the LNN. However, there were some issues that I want to post to you folks here and get your opinions. Here they are... "Meanwhile, time is ticking off and we have some pressure because I need stick time before Mike leaves in order to be able to continue to fly the airplane safely. The two remaining problems caused me heartburn: a baulky idle mixture circuit and a prop/governor problem. Both of which I would like help from the list with. The governor (McCauley unit from Lancair) problem surfaced when we tried a full power run-up to check static rpm. 2400 rpm was best we could do. No good. This is an IO-360 B1F with MT prop (MTV-12B). Target was 2600 rpm roughly. The prop would cycle normally however. Very unfortunately, I had some time ago removed the governor control arm to thin it so that the B-nut would fit on it. I realised too late that I had neglected to mark its position on the splined shaft and did not know where to put it back on. I guessed and flagged Mike about this. Figuring that I had put it back on wrong we moved it so that the governor would allow a higher engine rpm (rotate the governor shaft further into the body). We move it all the way to the limit and could do no better than 2450 rpm (?!) We took the governor to a prop shop and had it tested. It was about right at our final setting requiring the shop to tweak it only a little. Then the technician gave me the dredded "come hither" finger. He said the governor was flowing about half the oil it was supposed to. Yes, it was a new unit. Yes it was effectively on the shelf for a long time (2Q'97 build date). He said it should function normally but he wouldn't let one like this out of his shop. We put it back on the airplane and no luck, the rpm was not improved. Must be the prop (right?) MT has an easy way to adjust the blade pitch stops with a single nut on the front. We turned it and were finally able to get a satisfactory static rpm of 2600. Great, we're all set (yeah, right!) During the takeoff roll and into the initial climb the rpm climbed beyond 2700 and went well over. Mike was able to clamp it down with the prop control but we figured it went about 10% overspeed which sent us scurrying to the MT manual for consequences - fortunately only a 100 hour inspection. But why was our newly checked out governor allowing such an overspeed? We turned the prop pitch nut back halfway towards the original setting and found the overspeed was less. We found on subsequent runs that we could prevent overspeed by progressively pulling back the prop control during the takeoff run. We also found that we could not get more than a 10 or 20 rpm drop during prop cycling at the 1800 rpm runup. During flight the governor seems to control rpm normally in the range we used between 2200 and 2500 rpm and the position of the control seemed "normal" compared to what I had been previously used to. The rpm measurement was identical on the VMS unit and the separate rpm counter Mike had. Our conclusion: something's wrong with the governor. We base this primarily on the fact that the prop shop set it for 2700 max rpm (we watched this) and their statement that the flow rate was inadequate. Does anybody out there have a view that fits the evidence? If so, I would really like to hear it since we judge the airplane not flyable by me alone until this gets resolved. The second problem concerns the Precision fuel control unit. We are unable to get the customary 30-50 rpm rise during leaning at idle without running the mixture adjustment so rich that it jams against the unit housing during throttle application. We are also getting a lot of fuel seeping into the throttle body after shut down. We can tell this because the unit has been rotated forward with a 90 degree elbow attaching it to the bottom of the oil pan, so fuel tends to pool in the intake pipe in front of the injection unit. Additionally, when hot, the engine will diesel after the mixture is pulled for shut down and there is a lot of popping during idle which Mike described as "after firing". The mixture control screen was examined and found to be free of foreign material. This is a factory new Lycoming engine which spent an hour on the test dyno with this injection unit installed. All flight performance seemed to be normal. Our conclusion: the idle mixture plates inside the fuel control unit are worn or otherwise damaged. Can anyone shed any additional light on this? Best way to fix, etc. But back to the first flight... " and the rest you will have to wait for your LNN copy. For those of you not yet at this magical day, keep building and think safety. The airplane will reward you with a fabulous experience. Best Regards, Ed de Chazal >>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>> LML website: http://www.olsusa.com/Users/Mkaye/maillist.html LML Builders' Bookstore: http://www.buildersbooks.com/lancair Please send your photos and drawings to marvkaye@olsusa.com. >>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>