I thought I had chased down everything that could be coming in contact with
the cowling, but I still had a low frequency vibration that was in the airframe
and not in the stick.
In a discussion with Tom Giddings, he asked, "When did you last check the
engine mount to firewall bolt torques?" "Ah, probably two years ago," I
answered. Then I used some lazy man's excuse like "Well, I probably would
have checked them next month during the annual condition inspection." I
added, "The lower cowl is such a nuisance to remove."
Well, I did pull the lower cowl and used 5 drive extensions to get
a torque wrench socket thru the foot well to the
aft-side firewall nuts only to find that 5 of the 6 required 2-4
faces turned before the proper torque was restored (all three on the left
side, the middle and bottom on the right).
After re-assembly, I went for a test flight. I could tell that
things had improved just while taxiing out. One trip around the
pattern demonstrated that the low frequency frame vibration was gone (almost
reduced to nothing).
Remember that epoxy/glass/carbon can creep a bit under pressure and heat,
and it is wise to check the torque of these bolts periodically. Uh,
especially if vibration is beginning to felt where operations were once
smooth. This is relevant with any Lancair that has a composite firewall
(wood/glass, all glass, all carbon).
My 320 mount uses AN bolts that are 7/16" x 24 with a torque
range of 450 to 500 inch pounds (37.5 to 42 foot pounds). I used 40 foot
pounds.
Thanks again Tom,
Scott Krueger AKA Grayhawk