NTSB Identification: DCA84AA002 .
The docket is stored on
NTSB microfiche number 21244.
Scheduled 14 CFR Part 121: Air Carrier
operation of AIR ILLINOIS, INC
Accident occurred Tuesday, October 11, 1983
in PINCKNEYVILLE, IL
Aircraft: HAWKER SIDDELEY HS-748-2A, registration:
N748LL
Injuries: 10 Fatal.
ABOUT 1.5 MIN AFTER DEPARTING SPRINGFIELD, IL, THE FLTCREW REPORTED A SLIGHT
ELECTRICAL PROBLEM, BUT THEY CONTINUED ON COURSE. ABOUT 33 MIN LATER & A FEW
MIN BEFORE THE ACFT SHOULD HAVE REACHED ITS DESTINATION, THE ACFT CRASHED.
IMPACT OCCURRED WHILE THE ACFT WAS DESCENDING IN A RIGHT WING LOW ATTITUDE.
BEFORE CRASHING, THE PLANE'S HEADING HAD CHANGED ABOUT 180 DEG. A CVR TRANSCRIPT
REVEALED THE L GENERATOR (GEN) HAD FAILED AFTER TAKEOFF & THE 1ST OFFICER
HAD MISTAKENLYISOLATED THE R GEN. ATTEMPTS TO RESTORE THE R GEN WERE
UNSUCCESSFUL. THE CAPTAIN ELECTED TO CONTINUE TO THE DESTINATION RATHER THAN
RETURN TO THE NEARBY DEPT ARPT. THE CLD BASES WERE AT 2000' MSL, BUT ATC COULD
NOT PROVIDE AN IFR CLNC BELOW3000 FT. JUST BEFORE CRASHING, THE CREW INDICATED A
TOTAL LOSS OF ELECTRICAL POWER. THE L GEN DRIVE SHAFT HAD SHEARED. THE REASON
FOR THE R GEN NOT TO RESET WAS NOT DETERMINED. THERE WAS EVIDENCE THAT RECURRENT
FLTCREW TRAINING DID NOT PREPARE THE CREW TO UNDERSTAND & COPE WITH THE ELEC
PROBLEM & THAT FAA SURVEILLANCE DID NOT DETECT THE TRNG DEFICIENCY.
The National Transportation Safety Board determines the probable cause(s) of
this accident as follows:
IN-FLIGHT PLANNING/DECISION..IMPROPER..PILOT IN
COMMAND
SPATIAL DISORIENTATION..PILOT IN COMMAND
Contributing Factors
ELECTRICAL SYSTEM,GENERATOR..FAILURE,PARTIAL
ELECTRICAL
SYSTEM,GENERATOR..SWITCHED OFF
ELECTRICAL
SYSTEM,GENERATOR..FAILURE,TOTAL
SELF-INDUCED PRESSURE..PILOT IN
COMMAND
INADEQUATE RECURRENT TRAINING..COMPANY/OPERATOR
MANAGEMENT
INADEQUATE SURVEILLANCE OF OPERATION..FAA(ORGANIZATION)
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