Mailing List lml@lancaironline.net Message #44721
From: LHenney <LHenney@charter.net>
Sender: <marv@lancaironline.net>
Subject: LNC2 Hyd Chirp Tim/ Joe/ Brent Question
Date: Mon, 05 Nov 2007 10:55:23 -0500
To: <lml@lancaironline.net>

Scott,

 

As with most of which I speak, 90% was lost in my inability to articulate in a language perceptible to the soberness of my readers.  My point regarding the air in lines being an accumulator was missed.  I believe you dissected it below by pointing out the various natural paths by which air makes it’s way back to the pump.  I believe your premise was that all of the air gets back to the pump.  This would then make my premise that the air would act as an accumulator initially but thereafter work it’s way out.  Thus, one would have longer time between chirps (TBC) until the air worked it’s way out.  Then, ops normal (occasional chirpage ) would resume.

 

However………….  I rebuilt two main cylinders Friday and flew all weekend.  The results of much air introduced into the system were quite contrary to my theory.  It was pure chirpaholism for the first hour.  Thereafter, I ran the pump for about 30 seconds (dump valve open) upon each gear extension.  Now after 6 such cycles it seems to be “better”.  I need more cycleage to tell for sure. Or maybe more cylinders rebuilds.

 

BTW, does it bother only me that the HC-06 cylinder rebuild kit does not come with a thread seal?  I think a cylinder rebuild kit should include all the O rings and seals that the cylinder entails.  Especially, since our leak headache discussion is internal High/Low.  The seal is for the shaft at the piston.   It was only a minor set back  (90 mile drive and two hours at American Hydraulics with help from Rose).  Help us here Tim O., Joe  B.????  HC-06 no thread seal.  Is it the kit supposed to have one?  Mine haven’t several times.

 

On the secret switch note, I am one of those High pressure leaks to Low pressure side and sets low pressure switch guys (after some duration + 1 hr).  The opening of the dump valve, after the switch down does nothing, allows pressure off the low pressure switch and fires up the pump.  That’s why I keep going back to the shuttle valve test.  I find mine (once reversed) now in correctly.  The idea that both switches are set and anyone  CAN NOT get gear extension is beyond my fathom ability (ok, maybe the dump valve handle could fall off).  In other words, if the fluid is leaking to the low pressure side, then why do it not depressurize through the shuttle valve?  The pump would have been in the ……  (I don’t know?)??? BdBdBdBdBd (finger lapping against flapping lips)

 

On a parallel solution, my Berkut buddy (James Redmond) and all his Berkut friends use a different dump valve concept.  They say, yeah those little cylinders leak bad but we don’t care.  They dump both high and low pressure to a common line that returns through the center port in the pump.  I have such a port in my pump and wonder if this would be a safer Free Fall system.  He says the port is directly common to the jug and thus is a more guaranteed dump to ambient pressure. 

 

BTW, he bought a very nice little panel mounted valve.  The installation is soo much more professional than our knee knocker under sided Al flox blobbed chunk of workmanship.

 

The Berkut guys do several other little cutes like using Dexron III instead of 5606 and MOV’s on the pump wires.  I wonder sometimes about the shear stickiness of 5606 in my low pressure switch.  Is goo the problem?

 

Your secret wire with switch is interesting but perhaps I’d only have it on the down switch.  But, free fall works great.  Maybe with a three port dump valve, the secret wire to override a failed down pressure switch would be excessively redundant (like extra wings, prop blades, or prop bolts- you only need one, right?).

 

Still head scratch’n,


But at least my Catto Prop is soon to ship (RPM to follow).  Look out Bruce Hammer
J

 

Larry Henney

Race 36

252 mph Memphis 100 (wind enhanced)

 

PS:  And Brent, if photographing tail wind enhanced groundspeeds is analogous to standing on a pile of books, why does one arrive earlier as compared to the guy stepping off the books subsequently being his original height?  Flame suit worn out but ready anyway.

 

 

 


From: genemartin [mailto:genemartin@enid.com]
Sent: Sunday, November 04, 2007 9:28 PM
To: lml@lancaironline.net
Subject: Re: [LML] Re: FW: [LML] LNC2 Hyd Chirp Alternative Mousetrap

 

I have such a secret override switch...top secret unmarked don't ask don't tell.

Gene

----- Original Message -----

Sent: Saturday, November 03, 2007 9:06 AM

Subject: [LML] Re: FW: [LML] LNC2 Hyd Chirp Alternative Mousetrap

 

In a message dated 11/2/2007 10:48:32 A.M. Central Daylight Time, LHenney@charter.net writes:

Air is good if your breathing and bad if leaking into your brain.  OK, I'll go out and rebuild one this am and report back.  Oh, but wait, I guess the rebuild of the leaker will have an affect on our test. 

Larry,

 

I love spirited discussions leading to one's spirit sipping spirits during contemplation of the metaphysical.  I thought more about all the problems reported over the years and the possible effect of air.  Let's see if we can work thru this by picking the system apart.  But first, I said you should only introduce air into the system as a test of your theory, not rebuild a cylinder.  

 

Air in cylinders

 

4 of the six cylinders, those associated with the main gears and doors, can be eliminated because they are oriented horizontally with all ports pointed upward so the air will not remain in those actuators. 

 

The nose gear door cylinder, vertically oriented cannot hold much air in the bottom after extension because the air would have to fit in a donut cylinder volume 5/32 high with the inside 1/2" diameter and the outside 5/8 diameter - a volume of .017 cubic inches.  This space is inside of the extension piston stop that allows fluid to be passed in and out of the cylinder.  Upon retraction, even though the piston does not tightly reach the top, the fluid exit is at the top and air would be expelled.  The .017 ci of air could be trapped at the piston that is pushed in by the hi pressure retraction activity and the bubble could rise to the bottom of the piston.

 

The nose gear cylinder is somewhat vertically oriented and the cylinder cannot hold any air in the bottom beyond the piston at full extension since it is stopped tightly against the forward bulkhead (if properly rigged).  However, retraction is limited by the external stop and the fluid exit is at the aft lower side of the cylinder.  I forgot to check how vertically oriented the cylinder gets on retraction, but let's say the whole remaining space can retain air.  That is a cylinder approximately 3/4" high with a diameter of 9/8" for a volume of about .75 cubic inches.  Of course, at retraction this pocket would not be under pressure since it is the other side of the piston that is under pressure.  So, it is on extension that some of this pocket could be compressed although it would seem that some of the air would come out at each retraction. 

 

Air in lines

 

There also are short pieces of Easton flexible line that feeds into 1/4" hard Al lines. Let's discuss how much volume these lines can hold.  For the Easton line (I could not find a sample), assume it has an interior cross section of 1/4".   That is 20.37 inches of tube per 1 cubic inch of fluid volume.  The 1/4" hard lines have a wall thickness of .035, thus the interior diameter is .18" or 39.3 inches of tube per cubic inch of volume.

 

Door actuators move about .9 ci of fluid in when extended and .7 ci in when retracted.  The nose gear cylinder (I forgot to measure the length, say 4.5" of movement) moves about 4.5 ci of fluid in when extended and 4 ci in when retracted.

 

Since the opening of doors requires fluid passage thru sequence valves, those lines might not be completely cleared because of the hard line length may hold more fluid than is transferred to and from the actuator.  One could consider a small bubble remaining in those lines.  The retraction side moves more fluid thru shorter lines so it is less likely that air is trapped in those lines.  The large actuators move much more fluid and it is hard to believe any air remaining in those lines.

 

Air Elsewhere

 

The dump valve body can't hold air once it has been opened.  Perhaps the teed vertical lines leading to the pressure switches retain air.

 

Gas Laws

 

For those that suspect that heated trapped air raises the system pressure quite a bit should note that when the volume is held constant, the pressure increases as the temperature ratio, in Kelvin, increases.  A rise from 50F to 80F is 299K/283K or approximately a 5% increase - Hardly accounting for a rise of several hundred psi.  I await an engineer to evaluate effects of the differing expansion factors for aluminum, Easton lines, cylinders and the fluid itself.

 

On the converse, if the air is compressed (so far this looks like a problem that is possible solely on the down side at the nose gear actuator), I would finally have to agree that more volume of fluid under pressure from the air would have to pass through the system leak to activate the pressure switch than that from incompressible fluid on its own. Maybe.  That these air pockets may work themselves out so that the chirp rate increases is interesting.

 

So I can see where an accumulator could delay pump activation.  No problem as long as other parts of the system are working properly.  It is hard to see where any air bubbles could influence the up side of the system other than those trapped in the sequence valve circuits.

 

----

 

As to some of the other contentions.................

 

You said: "You're an electrics guy.  Does that little chirp every 20 seconds not bother you just a little?  You know, arcing and corrosion in the relays, airborne fire, alternator shorting, etc?"

 

You are correct, the wiring is correct.  Thus, arcing and corrosion are not a problem - intermittent relays are operating intermittently .  Airborne fire and alternator shorting are not a problem from the pump blips for the small percentage of block time that the gear is down, nor is anything else associated with the hydro-electric gear system.  However, "etc." does indeed bother me, although it is not related to this situation.

 

One of the risks you may add is that the accumulator on the high pressure side may lock up the low pressure side if you have a failure like that sometimes described by other Lancairites and not yet fully understood.  This is the case where opening the dump valve does not resolve the peculiarly built system pressure present on both sides and that trips both pressure switches.  There may be an electrical solution - perhaps bring duplicate wires from the pressure switches forward to secret over ride switches operable by the captain.  Forced activation of the pump may free the lockup if it is the case of a stuck shuttle valve.  Of course the captain's hearing has to be good enough to perform an "undo" if the pump is straining as the captain becomes the acting pressure switch.

 

Good Luck,

 

Scott Krueger AKA Grayhawk
Lancair N92EX IO320 SB 89/96
Aurora, IL (KARR)

Darwinian culling phrase: Watch This!




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