Return-Path: Received: from pop3.olsusa.com ([63.150.212.2] verified) by logan.com (CommuniGate Pro SMTP 3.5b3) with ESMTP id 856432 for rob@logan.com; Thu, 23 Aug 2001 14:53:42 -0400 Received: from imo-m07.mx.aol.com ([64.12.136.162]) by pop3.olsusa.com (Post.Office MTA v3.5.3 release 223 ID# 0-71866U8000L800S0V35) with ESMTP id com for ; Thu, 23 Aug 2001 13:17:24 -0400 Received: from AVIDWIZ@aol.com by imo-m07.mx.aol.com (mail_out_v31_r1.4.) id k.12c.37e33a4 (15891) for ; Thu, 23 Aug 2001 13:27:49 -0400 (EDT) Received: from web48.aolmail.aol.com (web48.aolmail.aol.com [205.188.161.9]) by air-id08.mx.aol.com (v80.17) with ESMTP id MAILINID86-0823132748; Thu, 23 Aug 2001 13:27:48 -0400 Date: Thu, 23 Aug 2001 13:27:48 EDT From: AVIDWIZ@aol.com Subject: Followup on Crash of N424E To: Mime-Version: 1.0 Content-Type: text/plain; charset=ISO-8859-1 Content-Transfer-Encoding: 7bit Message-ID: <12c.37e33a4.28b69714@aol.com> X-Mailing-List: lancair.list@olsusa.com Reply-To: lancair.list@olsusa.com <<<<<<<<<<<<<<<<--->>>>>>>>>>>>>>>> << Lancair Builders' Mail List >> <<<<<<<<<<<<<<<<--->>>>>>>>>>>>>>>> >> Gentlemen of the list: The memo will update you on the developments on the crash of N424E, a Lancair IVP, ser #11 built by John Kerner which crashed in Flagstaff AZ, June 16th killing the pilot Tony Durizzi. As you recall, he crashed 2 miles short of the Flagstaff airport after a flight from Ada, OK which lasted 3hr 13 min at FL 220 in VFR Conditions. The engine was not running at the time of impact and based upon his distress call just prior to the crash, while on a final approach he lost his engine and was forced to make an emergency landing. Fuel was found in the lines and spider valve under pressure. Subsequent to the crash, a Lancair factory representative along with the FAA and NTSB inspected the wreckage and determined that a fuel vent for one of the fuel bays in the leading edge of the right wing had been omitted. Additionally, it was determined that during the closing of the left wing, resin had dripped onto the slosh door and restricted it from having full movement. The forensic data report commissioned by the NTSB from Archangel Avionics on the contents of the memory chip in the EFIS has been obtained. The results are that the fuel totalizer showed 14.6 gallons remaining at the time of impact. Previous testing of the EFIS fuel totalizer by Tony and myself showed that it was accurate to within 2% (i.e. 1 gal per 50 gal fuel load usage). As a part of the pre-start checklist we entered the full fuel capacity once the plane was topped off so it is reasonable to assume that the totalizer started with 80 gal. These numbers indicate a total fuel burn for the 3.25 hr flight of 65.4 gal or 20.12 GPH which are in line with tested performance results for this aircraft. In January 2001, Tony checked the fuel capacity of the plane by draining the tanks and re-filling them. The actual original fuel receipts and his notes have been located and demonstrate that a total of 80.5 gallons were possible to be carried on board. Prior to departure from Ada, OK witnesses saw the plane topped off which was confirmed by the FBO. Clearly Tony was under the impression that there were 80 gals of fuel on board. We know this from the fact that Tony went into exhaustive detail documenting the fuel capacity testing which included draining and re- filling each tank as stated above. However, we can now determine that some 14 gal were un-usable. This 14 gal can be accounted for by virtue of the 9 gal held in the right wing fuel bay which was blocked from being usable by the missing vent, 2 gal normally un-usable in a IVP and the remaining 3.6 gal a combination of a gauge error (2% = 1.6gal) and/or fuel which was un-usable due to un-porting caused by the restricted slosh door in the left wing. I realize that many of the members of the list have voiced the opinion that this crash was due to as much pilot error as anything. While I understand the natural inclination to want to believe these planes we build and fly are safe and the mistakes of others will not be repeated by ourselves, I have to point out that this accident could have happened to any one of us. While it is true that Tony was aware that the aircraft had fuel system problems, he had every reason to believe that he and the builder had repaired those problems. He was able to put a full 80 gal in the tanks whereas prior to the repair this was not possible. However he never had any idea that 14 of those 80 gals could not be delivered to the engine ... something many of us would have missed as well. I hope this information is of use and that it will cause us all to look closely at the planes we fly to determine weaknesses before they rise up and bite us. Regards, Dave Riggs >>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>> LML website: http://www.olsusa.com/mkaye/maillist.html LML Builders' Bookstore: http://www.buildersbooks.com/lancair Please send your photos and drawings to marvkaye@olsusa.com. >>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>