X-CGP-ClamAV-Result: CLEAN X-VirusScanner: Niversoft's CGPClamav Helper v1.23.0 (ClamAV engine v0.103.0) From: "Stephen Izett stephen.izett@gmail.com" Received: from mail-pl1-f175.google.com ([209.85.214.175] verified) by logan.com (CommuniGate Pro SMTP 6.2.14) with ESMTPS id 1240821 for flyrotary@lancaironline.net; Sun, 21 Feb 2021 02:49:39 -0500 Received-SPF: pass receiver=logan.com; client-ip=209.85.214.175; envelope-from=stephen.izett@gmail.com Received: by mail-pl1-f175.google.com with SMTP id d11so789748plo.8 for ; Sat, 20 Feb 2021 23:49:41 -0800 (PST) DKIM-Signature: v=1; a=rsa-sha256; c=relaxed/relaxed; d=gmail.com; s=20161025; h=from:content-transfer-encoding:mime-version:subject:date:references :to:in-reply-to:message-id; bh=Y2WfPF8pWa5yPwfogSEdZGm46giUuaA6u4dW7TTbiYg=; b=rZfQYb7L/RhM/Fnl+oaMBL0FMZqkjC6HsViN+MBYbc3YV4oebETxhzvKk3Cnm8WImP bZ4ZvOH1zfrwXMiEAtt3MTNVFSR6dnxtWDxc3CZ2+6vCS8WmxT75Ha2HzA4w9WWlA5Lt csm3gM4yPzLzd5bMSt4EI64YPaYl0oWy8jl5/EoRBxyNEeKFXDk/5MghKyGd9F4qY9SW 0IVluyZB5yZRsMm5XUo1rTWyW088/mxsxVmi1x1QpxcnsSqG5Dd/suGi0fr/jmFd89BH J3abrErdWh9plLwJgHmfaUEyIzdjdzPTARcLLHcOdjhrooCldHx1ieQNM2UAQL9s+rlf 0n2w== X-Google-DKIM-Signature: v=1; a=rsa-sha256; c=relaxed/relaxed; d=1e100.net; s=20161025; h=x-gm-message-state:from:content-transfer-encoding:mime-version :subject:date:references:to:in-reply-to:message-id; bh=Y2WfPF8pWa5yPwfogSEdZGm46giUuaA6u4dW7TTbiYg=; b=Q1yqUu67aoqM/blW6te41HamWccqd5FcVhei9U9UWDAPJeFxzlmphTqz1QyjAt15sF VfhNI7l7t4D1igY4RzvfW0zOZ57cU7vyIFiGt5/hZeOASxYABpftXDsH8rh6sKTdiFQ5 o93TzygAgGQWOvKE10XBUFEepyf1VJiTOt955nFJEKTYz+yWa6BRguXmiQdQVWfRc3p+ LEr7/gNYJ1oslpqZwKTLVwtmf8ZwcGm4GE7DY6MzEpe/MX1SeWgoq4tg0Qpi3g8B1wXv kbsqzsf4PD7mDozXbWw/GrKKHErT+4BHjhg7cGgQfdeL4fsxR2F7555hhl3F68lbcBCw 0VpA== X-Gm-Message-State: AOAM531Zw203pyAuOYHPT1QJ37SZb3ARJvwQQMg0uA3kelCdvhySn2Lz lZkWzDzmoi+knCxEjkrq4hMUu5K0baE= X-Google-Smtp-Source: ABdhPJzkyn9tAMqUocQRp+bcVsp6fSwZPqIcTdZdwx0Rk1wloC1NAxPgwGjcRrMOcdMvFoNjmviX2A== X-Received: by 2002:a17:90a:4fc1:: with SMTP id q59mr17860852pjh.129.1613893763220; Sat, 20 Feb 2021 23:49:23 -0800 (PST) Return-Path: Received: from macbook-pro.lan (220-235-124-195.dyn.iinet.net.au. [220.235.124.195]) by smtp.gmail.com with ESMTPSA id h23sm14864131pfn.118.2021.02.20.23.49.21 for (version=TLS1_2 cipher=ECDHE-ECDSA-AES128-GCM-SHA256 bits=128/128); Sat, 20 Feb 2021 23:49:22 -0800 (PST) Content-Type: text/plain; charset=utf-8 Content-Transfer-Encoding: quoted-printable Mime-Version: 1.0 (Mac OS X Mail 14.0 \(3654.60.0.2.21\)) Subject: Re: [FlyRotary] N214FL RV-4 First Flight Date: Sun, 21 Feb 2021 15:49:18 +0800 References: To: Rotary motors in aircraft In-Reply-To: Message-Id: <76AB10B3-7FD7-4CB4-87EB-48E9B4E1F4D1@gmail.com> X-Mailer: Apple Mail (2.3654.60.0.2.21) Hi Finn I see that I was reading your water temps wrongly. You were a little = warmer than I first thought. The pressure transducers I am using are MPX10=E2=80=99s. I=E2=80=99m = using 5 that I purchased on eBay. They are probably not true Freescale = units but Chinese ripoff=E2=80=99s I=E2=80=99m guessing. I started wiring them directly to the EGT inputs with the dynon = providing the 5v supply. =46rom memory Ive now added 1K in each leg. I just used Cat 5 twisted pair cable so the signals are noisy but = readable. Engine Monitor is in the cockpit while box of stacked transducers are = under the cowl in the heat. I=E2=80=99m using them with the differential inputs across the face 4 = inches in from each corner and one in the middle of the core. Wish I had a bunch more for higher resolution of the face, but this = gives me some picture of the pressures. A couple of issues: 1. When I tried to calibrate them with a water manometer to read inches = of water on the Dynon they max=E2=80=99d out at about 6 inches H2O. The = data sheet says 1.45 psi which I thought was 40 inches of H2O. I=E2=80=99m just not sure what the EGT input circuitry thinks of the = transducers output impedance etc. or the temp compensation. 2. Ive had issues with a couple of the transducers now in flight. As in = the data going haywire. Sometimes providing constant data but then at = other times all over the shop. I thought it was temp related, however I=E2=80=99m beginning to suspect = that there is substantial turbulence inside my diffuser. Either way, they still have given me comparative data which has been = very illuminating. On the last test after squeezing the wedge end really tight the upper = back transducer reported very low pressure (As in, the diffuser wall is = now against the radiator face and there is now basically zero flow to = that 4 x 4=E2=80=9D section - perhaps larger). Having changed the shape of the diffuser, the flow through the front of = the Rad has improved enormously. The result better cooling than previous = flight data ever with that back corner section not flowing any air! So I=E2=80=99m going to sand off some of the foam in the diffuser and = open up the end of the wedge slightly, and hope to improve the cooling = even further. Cheers Steve > On 21 Feb 2021, at 11:50 am, David Leonard wdleonard@gmail.com = wrote: >=20 > Congratulations Finn! > You must be walking on clouds. >=20 > I agree that more cooling will make flying more enjoyable for you. = Getting cooling capacity at exactly the optimal level is very tricky. = So I say error well on the side of excess cooling. Makes life easier, = makes flying more relaxing, and the loss in performance is practically = trivial. >=20 > Dave Leonard >=20 > On Sat, Feb 20, 2021, 11:25 AM Finn Lassen finn.lassen@verizon.net = wrote: > N214FL left the ground this morning for an 18 minute flight. >=20 > Main concern was engine (water) cooling. As you know, cooling is a = compromise between drag from unnecessary air through cowling and = adequate cooling during normal flight conditions. Climbed to 1,500' = before pulling back on throttle to see if coolant temp would stop = rising. It did. Still, I think I erred in too small fluid inlet openings = in the A/C evaporator cores I used for radiators. Some more work in that = area is in my future before hot days arrive. >=20 > Cut the flight short due to a bit of smoke (didn't smell anything) = briefly observed low in the cockpit at full throttle later in the = flight. To be investigated.=20 >=20 > Van's RV-4 with Mazda 13-B Renesis (RX-8) stock engine. > RWS 2.87:1 Propeller Speed Reduction Unit > RWS Engine Controller and Monitor (modified) > Performance Propeller 76x88 > Empty Gross: Approx 926 lbs. >=20 > Engine log attached. Unzip and open with Excel. >=20 > WTALR: Water temp after left radiator > WTARR: Water temp after right radiator > Use EGT and CHT Ref to compare to OAT and adjust accordingly. >=20 > Finn >=20 >=20 >=20 > =09 > This email has been checked for viruses by Avast antivirus software.=20= > www.avast.com >=20 >=20 > -- > Homepage: http://www.flyrotary.com/ > Archive and UnSub: = http://mail.lancaironline.net:81/lists/flyrotary/List.html