Besides SS bends from
stair rail, the dairy industry and wine industry (food processing)
also have some nice SS bends available for an exhaust system. I
made my own SS flanges and TIG welded.
Terry
Charlie is correct. Cut the header tube a few inches longer then
you think you need and inspect. You should be able to insert your
tube between the outside SS shell and inner inconel tube. Trim to
fit and lap joint weld to the outer shell.
Bobby
Sent from my iPad
You
know they are 3 layers thick, right? I've cut one up,
and modified another that's attached to my engine now,
though it' hasn't run yet. I suspect that the inner
liner is inconel, but I tig welded some stainless to it
using stainless rod. The flange is cast iron, with the
inner core probably inconel, 'something' over that, and
the outside seems to be stainless.
Dennis
Haverlah has been flying one for a long time; perhaps
he'll chime in with what he used to modify his.
If I
were starting today, I'd probably just use the flange
and make up a header out of thick wall stainless tubing
bends (meaning architectural guard rails). That's what
Ed Anderson did a couple of decades ago on a much hotter
running 13B, and it survived fine. Right, Ed?
That
manifold is pretty heavy. I used it because Dennis'
plane was so quiet you could hear the prop. Then I heard
Sam Hodges' plane that has a welded header, and it's not
much louder than Dennis' plane (both are Renesis
engines).
Charlie
Andrew,
I spent a lot of time chasing
temps, even after supposedly calibrating with a
thermometer. IN the end I found a bloke who simply
took the number off the sender and put the relative
values into the computer. They nearly all read
differently. The difference in my two oil temps is
confusing, as in theory should read almost the
same. I no longer care but remain confused which
seems normal for me.
Does anyone know what type of cast is the stock
renesis exhaust manifold made from? I normally use
Procus welding rods for dissimilar metals, which to
date seem to stick even a broken marriage together.
A delight to weld with as they flow so smoothly .
Not cheap but the job even makes my welding look
good.
Neil.
Hi Neil, I dont remember
criticising, but maybe I did. Anyways your setup
works, thats all that matters.
Keep us updated with the turbo
install. Tis fun to tinker, but more so to fly.
Pulled my oil filter & adapter
plate off this arvo, realised the temp sensor that
is reading high is not completely in the oil flow,
just the very tip is, with rest of sensor in
contact with adapter plate, so maybe I’m sensing
the rear iron temp rather than oil temp. would
explain a lot, and be a bugger, as I may not have
had oil cooling issues at all for all this time.
Andrew
Andrew,
I think it was you who
condemned my remote filter as
undersized, anyway someone did. I have a 3/4
inch inlet size and out
but sized down to 1/2 inch lines to and from.
Oil pressure at cold is
120 psi and runs at 85 when hot or slightly
less. I have one temp
sensor in the back iron where Mazda put theirs
and another one in the
reduction drive. Temp in the reduction drive
is always higher than the
one in the rear iron as I suspect water is
aiding that reading. Get up
to 95 degrees in the reduction drive and only
85 to 90 in the rear iron.
Have just a pressure reading post filter.
It seems happy, so I am
just flying.
Have a stock exhaust manifold coming to see
what I can do to reverse the
direction and then fit a turbo. Yeah I should
be shot I know, but just
cannot stop fiddling. Will fit to another
engine on the floor and then
hopefully the change over will not ground me
for long. I have an
operation on my foot in Mid March which means
I am grounded for 6 weeks,
so me and my crutches should get the change
over done in that time.
Best for new year! Neil
On 1/3/2019 3:19 PM, Andrew Martin andrew@martinag.com.au
wrote:
> Really think I’m starting to win. But
very slowly, which is
> frustrating. Seems my initial overheating
issues were a combination of
> many things, not each that bad in
installation but added together!!!!
> and each masks the others.
>
> Mocal oil cooler definately works, and
judicious application of duct
> tape over all the now unnecessary holes
in the cowl to improve airflow
> seems to have done the job, and can now
be done proper again with grp.
>
> But. Seems my oil filter is next on the
list to address. I used the
> stock mazda renesis oil filter. It
actually looks too small to use (
> which I now believe it is) but I stuck
with it because I assumed
> mazda did the calculations ( No, the
accountants probably took over).
> Mazda’s filter setup only filters oil
going to the oil galleries, most
> oil is not filtered and just returns to
sump via the OCV. Since
> fitting new oil cooler I now also have 2
temp sensors, both after the
> oil cooler but original 1 is also after
the filter. Both are on rear iron.
>
> On latest flight, oil going to OCV max’d
at 176f while filtered oil
> going to oil gallery/rotors kept climbing
to 216f where I aborted the
> climb. Couldve kept going as temp started
to behave as I reduced
> climb, but I really want to fix these
little nuances that restrict
> performance. Maybe something unknown is
affecting the sensor,
> otherwise it has to be the filter.
>
> So, 2 choices, either a better filter
that just filters gallery/rotor
> oil, or a remote filter that filters all
oil.
> If using remote filters, what size/part
number do you use? Has anyone
> measured presure drop/ restriction
through filters?
>
> Andrew
>
>
>
>
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Andrew Martin Martin Ag
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