The following observations may be of interest in the light of
recent discussions.
On the flight to the resent Rotorfest, I thought the exhaust
noise level had increased at one point. This was just chalked up to
fatigue and the longer than normal time in flight since this was the longest XC
attempted to date. My usual procedure for adjusting throttle position is
to advance it until no further increase in rpm results even though there is
normally about ¼ of the total travel still available. My throttle body is
a cut down Mazda one with two openings as described in Tracy’s guide. Since I use the stock
oil metering pump, the throttle position adjusts the metering pump stroke and
advancing the throttle more than necessary results in accumulation of oil in
the sump. At one point when checking the throttle position, the RPM
actually dropped slightly when advancing the throttle further. I thought
to myself “this is strange” and returned the throttle to its
original setting since things were running smoothly.
At the Rotorfest, I listened with interest to Mark’s
presentation on muffler lifetime or lack thereof, wondering why my first
attempt at a muffler had survived so long. I attributed this to my normal
operation at high density altitudes which results in reduced max power levels.
I also described the construction of my “bomb” to several people
who were interested in it. I now realize that I didn’t know what
was in it myself. During the preflight before leaving the Rotorfest, I
noticed a rattle in the muffler when checking its security to the belly of the
plane. After returning to Laramie,
I investigated the rattle further and the results are shown in the attached
pictures. The fact that the center baffle broke is not surprising since
it was simply a push fit into the shell and was vulnerable to flexing since it
was flat. The repair uses a conical shaped baffle with a solid ring
around its outside circumference to make it even stiffer. We’ll see
how long that lasts.
The recent discussion on not developing full power,
especially Ed’s information on seeing almost 20 gph at max power settings
at seal level got me thinking about my performance. I have seen up to 16
gal/hr at 4500 ft DA on a rare excursion to that low an altitude. That
didn’t seem unreasonable considering the sophistication of my setup
compared to Ed’s. Looking back at the data log from the flight home
from the Rotorfest, there were some interesting observations concerning the
departure from 40XS. That segment of some of the data from the log is
shown in the attached plots.
A couple of things in the data seem to me to stand out.
One is that I am recovering nearly full manifold pressure in the plenum at wide
open throttle compared to ambient as shown in the data of the manifold pressure
before start-up and during runup and take off. This has always been the
case. The second thing that stands out is that I was only using between
10 and 11 gal/hr at wide open throttle with the mixture adjusted for max
power. I didn’t look at the fuel flow reading during runup or take
off and only noticed these low values when examining the data log
recently. I am confident that the fuel flow readings are quite accurate
since the fuel actually used for this trip matches the instrument readout very
well. While some of you may have experienced some apprehension at such a
pathetic power production level, it seemed normal to me since I usually operate
at density altitude from 7000-10000 ft. Another thing I noticed in the
data is the significant rpm drop when the prop unstalled just prior to liftoff.
The rpm usually drops a little at that point but not nearly this much. I
remember noticing this on departure, but was otherwise occupied and
didn’t give much further thought at the time. Not shown in the
plots is the coolant temperature which reached 225 degrees at the stock
location in the flywheel end iron at 8 minutes into the log. This is
about 20 degrees higher than normal even at the reduced fuel consumption level
during this time. Oil temperature showed a similar response.
After removing the muffler to investigate the rattle,
standing it on end would allow the broken segment to move to the area of the
outlet and block some of the exhaust exit area. Laying it horizontally
again would allow the broken segment to slide down the conical end where it
could not be seen in the exit. I suspect that the exhaust gas carried the
broken segment up the slope where it could block part of the exit when
operating at power levels above idle. Luckily, the blockage was not
enough to prevent generating enough power to sustain flight.
In any case, the data log is a record of the effect of
increased back pressure on the performance of my NA 13B. Just as has been
described in the recent discussions, the result was as expected: decreased max
fuel consumption and decreased max power production. In addition, I saw
increased coolant and oil temperatures. Maybe the increased back pressure
was responsible for the decrease in rpm upon fully opening the throttle in
stabilized flight, but I’m not sure why such an effect would arise.
For what it is worth…
Steve Boese