Jerry,
You could be right there with the higher velocity -
but I was referring more to the lower velocities, bigger tubes
scenario.
George (down under)
George,
just a reminder that the "fuel droplets dropping out of suspension" is just a
theory that may or may not actually occur or even if it does occur, may not
have much of an effect. At the velocities we are talking about, the inlet
charge may well scrub off pipe interiors preventing any build up. If this is a
real problem then moving the injectors to the bottom of the sweep just in
front of the throttle body should take care of it. Direct injection may turn
out to be an elegant solution to a problem that does not exist.
Jerry
On Thursday, February 10, 2005, at 03:00 AM, George
Lendich wrote:
Tom, Your on the right track! Exhaust
contamination of the inlet charge, affects idle ( only) as the exhaust
become self evacuating at higher velocity (RPM). Cause larger Ports and
PP Backpressure on the inlet charge also affects idle as the
backpressure cause fuel droplets to drop out of suspension, which causes
surging, one inlet charge lean the next rich etc. Cause larger ports and
PP. The close to housing butterfly, helps to minimize both,
before too much ( of either) enters the inlet manifold
tube. The RX 8 eliminates the first problem i.e.
overlap. No problem with the second. PP can cause the second
problem. DI will eliminate both problems! George ( down
under) Sorry. Ok, it's not the residue that would be a
problem, it's the back pressure in a combined intake system.
Tom
<tomtugan@yahoo.com>
wrote:
That is interesting Ed. Just thinking about it and
now it would seem that the expelled residue would be the first thing
that got sucked back thru a dedicated runner, also having a negative
effect.
Ed Anderson <eanderson@carolina.rr.com>
wrote:
Tom, One
reason that Jerry would not want to do that is that there is overlap between
intake and exhaust. That means while one rotor is trying to suck air
in its intake port - the intake port of the other rotor may be expelling
some residue exhaust gas out its intake and opposing any incoming air.
I think the engine would certainly run but I don't think you would
develop best power. Now it would probably be a different
story with the Renesis which by moving the exhaust ports to the side
housings has eliminate the exhaust/intake
overlap. FWIW Ed
A
----- Original Message
----- From:
Tom To: Rotary motors in
aircraft Sent: Wednesday, February 09, 2005 8:58
PM Subject: [FlyRotary] Re: P port intake
Jerry, Since
only one rotor chamber is drawing fuel/air at any given time, why would you
not feed them both from a single throttle body? Tom
Jerry Hey
<jerryhey@earthlink.net>
wrote:
George, originally I was going to hook up with a piece of hose
over the butted pieces with a couple of hose clamps. That is how I will
attach the other end at the throttle bodies. But, we have been
considering welding and also building some type of flange. Certainly, for
starters I will use the hose and clamp method.
Jerry
On Wednesday, February 9, 2005, at 08:43 PM,
George Lendich wrote:
> Jerry, > Is that a but weld, OR
does the tube go into the bellmouth end OR a > flange that they
both go into. > George ( down under) > > -----
Original Message ----- > From: Jerry Hey > To: Rotary motors in
aircraft > Sent: Thursday, February 10, 2005 9:35 AM > Subject:
[FlyRotary] Re: P port intake > > Yes, it is 1.61
inches. > > > On Wednesday, February 9, 2005, at 05:39 PM,
Tom wrote: > > Jerry, > Do you have an i.d. measurement
for the narrow end? > > TIA > Tom > >
Jerry Hey wrote: > > Today UPS brought the bell mouths for the P
port intake. They are > three inches o.d. across and have a smooth
gradual taper down to the > runner size
... > > > > > > > Do you
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